Dragy the dailys and mistakes may have been made . . .

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  • เผยแพร่เมื่อ 21 พ.ย. 2024

ความคิดเห็น • 6

  • @HankeyMountainGarage
    @HankeyMountainGarage 2 ปีที่แล้ว +1

    How much HP is that 351 making?

    • @blueovaldude
      @blueovaldude  2 ปีที่แล้ว +1

      Funny story about that engine. I actually don't know . You can go back to some of my earlier videos and I tell what happened. #3 intake port pushrod pinch broke through on the dyno . Pulling in enough oil to not fire on that cylinder. Among the top end filling with oil and dropping oil pressure at 5500 . Perhaps partly due to vacuum from #3 broken port (experimental fairly extreme port work ). So it was only running on 7 cylinders at the time . Only Running it to 6,000 made 496ftlb at 4,900 and 473HP at 6,000 . And so it came off the dyno to fix the issues . Make the pushrod pinch thicker and offset the rockers more , add oil restrictors , scallops in the windage tray idk a bunch of other things . Anyway I didn't dyno it after everything. It's in the car now . On the motor I expect 520-530 HP . It's really put together for some power adder action. 😉

    • @HankeyMountainGarage
      @HankeyMountainGarage 2 ปีที่แล้ว

      @@blueovaldude were you able to reuse those heads you ported or did you have to get new ones?

    • @blueovaldude
      @blueovaldude  2 ปีที่แล้ว +1

      @@HankeyMountainGarage yes , they are on the engine now . I offset the rockers .210 and I re-did every pushrod pinch as to put more material back . There is literally no pushrod pinch in the heads . All the specs , dyno sheet , mods ect are all in earlier videos.

  • @chestrockwell8328
    @chestrockwell8328 2 ปีที่แล้ว +1

    BOD, sorry to learn you've lost some channel content, gotta be aggravating. See you on the next one.

    • @blueovaldude
      @blueovaldude  2 ปีที่แล้ว

      Thanks, yeah it was frustrating to find out it was all gone .