HOW TO: JUNKYARD M90 BLOWER ON A 5.3L Z71 SILVERADO-WHAT WENT WRONG? WHY DOESN'T IT MAKE POWER?

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  • เผยแพร่เมื่อ 15 ม.ค. 2025

ความคิดเห็น • 408

  • @adamadriano9957
    @adamadriano9957 11 หลายเดือนก่อน +9

    I don’t know how you don’t have more subscribers!! Content is too good!

  • @keithbarron3654
    @keithbarron3654 11 หลายเดือนก่อน +20

    V mounted Knock sensors could be picking up blower rotors, pulling ignition.

  • @DangaRanga
    @DangaRanga 11 หลายเดือนก่อน +26

    Honestly, I've seen enough of those coils die, that swapping the coil from a good cylinder to #7 to see if the problem follows the coil would have been high on my list after verifying everything was reconnected properly and in the correct locations.
    I believe those early year trucks get pissy if theres a poor ground to the coil pack via the mounting bolt. maybe due to age and fussing around in the engine bay, you disturbed the little connection it had. Could stick a power probe to it while loaded to provide direct ground and see if it improves. Sometimes its easy to look past the simple stuff

    • @lafinrat
      @lafinrat 11 หลายเดือนก่อน +1

      None of the Gen 3/4 coils ground through the mounting bolts. The coil brackets and valve covers are insulated from ground.....

    • @pmotorsports8276
      @pmotorsports8276 11 หลายเดือนก่อน

      Every coil that I found bad = we're physically broken or aftermarket.

  • @harrison2281
    @harrison2281 10 หลายเดือนก่อน +9

    Put the hood in service position! That hood can be opened to a full 90° by simple moving 2 bolts. Wouldn't have had to be hunched over so far during intake and blower install. GMT800 Easter egg is hood service position

  • @Turbogto_guy
    @Turbogto_guy 11 หลายเดือนก่อน +3

    I admire the amount of work you went through to make this video happen.

  • @2wheelzdown180
    @2wheelzdown180 11 หลายเดือนก่อน +12

    Run a scanner on it and see how many counts of misfire you’re getting. Had a 6.0 with small crack in exhaust manifold that was barely noticeable unless u were almost against manifold listening . No cel ,good o2 reading, . Kept throwing misfires on 7 and slight across the board on that bank . Welded it up and it cleared out them all . Just a thought

  • @70sAirForceBrat
    @70sAirForceBrat 11 หลายเดือนก่อน +20

    Rich, are we ever going to see the m90 on a 4.3 V6 Vortec? Rich, there is an Astro van or a express van with a 4.3 in it with your name on it at your favorite U pull it.

  • @hardhead7056
    @hardhead7056 11 หลายเดือนก่อน +7

    Dont give up. Power through. Definitely following.

  • @kriskoch1462
    @kriskoch1462 9 หลายเดือนก่อน +3

    Richard,
    Bud, DONT GIVE UP ON THIS!!! I CANNOT WAIT TO SEE this work I have the same truck with a 5.3l59 with AFR heads, truck Norris, Fast intake, 90mm tb, headers, 36lb injr, 4.11 front/rear it screams! Lol

  • @sigvision4189
    @sigvision4189 11 หลายเดือนก่อน +30

    Don't realize how heavy a supercharger is until you have to lift out over the engine to put it in its home.

    • @lifeishard1211
      @lifeishard1211 11 หลายเดือนก่อน +2

      the gen 5 I just bought weighed like 30 lbs.

    • @sigvision4189
      @sigvision4189 11 หลายเดือนก่อน +1

      @lifeishard1211 Yep, I have a gen 3 and 5. Not bad until you are bent over front and trying to set them in place. Not bad if you can get in engine bay but mine I couldn't

    • @bcbloc02
      @bcbloc02 11 หลายเดือนก่อน

      Maybe your catalytic converter is stopped up and it just won’t flow anymore so the added boost is killed by extra exhaust back pressure and the power to turn the blower?

  • @hydrocarbon82
    @hydrocarbon82 11 หลายเดือนก่อน +10

    The 'heatsink' d585 coils have lately become a common problem. I had one turbo truck where 2 weren't firing, and another that literally blew the bottom out as we were warming the truck up prior to tuning. A friend also had them on a 6.2 that blew up, we suspect from 2 firing early due to overheating (self-protection). You'll still get spark, but being so early it either knocks or kills power like it's a dead cylinder.

  • @MrJustinWheeler
    @MrJustinWheeler 11 หลายเดือนก่อน +10

    Can’t wait to see what you figure out. Good luck!

  • @scotttimpany2845
    @scotttimpany2845 11 หลายเดือนก่อน +5

    Whoa! I thought for sure you were NOT going to stick the landing @ 5:38.

  • @sstevocamaro
    @sstevocamaro 11 หลายเดือนก่อน +6

    Did you put intake manifold gaskets on? It didn’t look like it..

    • @justinwhitaker6128
      @justinwhitaker6128 11 หลายเดือนก่อน +3

      I didn’t see any intake gaskets go on either.

    • @gearjonny369
      @gearjonny369 11 หลายเดือนก่อน +1

      I saw the same.. but sure didn’t want to be the one who asked!

  • @baby-sharkgto4902
    @baby-sharkgto4902 11 หลายเดือนก่อน +5

    Did OJ cut the plug wire?

  • @jeremymardlin5381
    @jeremymardlin5381 11 หลายเดือนก่อน +11

    It wouldn't be the first time I've seen a coil spark a plug outside of the cylinder and not wotk under cylinder pressure.

    • @bobroberts2371
      @bobroberts2371 11 หลายเดือนก่อน +5

      Champion made a plug cleaning / testing machine back in the 1960's or earlier. There was a spot to screw the plug into then you applied air pressure to see if the plug still sparked when you looked through the little glass window.

  • @davebarnes1370
    @davebarnes1370 10 หลายเดือนก่อน +3

    Fix that thing Richard! Can't leave us hanging??

  • @theone861
    @theone861 11 หลายเดือนก่อน +2

    I had a "The Other Guys" idea. How about a comparison between a Chevy 265 vs. Pontiac 265. I believe they have the same bore & stroke but I wonder how they'd respond to similar upgrades. I know it's a long shot since they're both ancient engines. Keep up the good work.

  • @derekfelber743
    @derekfelber743 11 หลายเดือนก่อน +3

    Are you confident that the injector plug was making contact with the pins in the injector? Ive seen cheap plugs be janky and have issues making connection with pins. Could pup that rail out and crank it to verify spray out of all injectors

  • @josephschaefer9163
    @josephschaefer9163 11 หลายเดือนก่อน +3

    Check your spark arc length. I've had coils fail that still sparked. Car made about 50 hp til I changed coil packs

  • @chrishansen7004
    @chrishansen7004 11 หลายเดือนก่อน +1

    spark plugs and coils? this is quite the pickle you got yourself into richard! cant wait too see the rest of this project!

  • @Tyler-fi4ms
    @Tyler-fi4ms 11 หลายเดือนก่อน +1

    Richard i love your videos! Have you ever thought about doing a dyno comparison on different turbo compressor housing designs?

  • @scottc74
    @scottc74 11 หลายเดือนก่อน +3

    Did you check for slippage in the trans., and just in case, did you change the torque management settings in the "ECM/TCM"?

    • @yeahididit9054
      @yeahididit9054 11 หลายเดือนก่อน

      Ish was in the driver seat doing the tuning 100% that’s correctly done

    • @jongoin4404
      @jongoin4404 8 หลายเดือนก่อน

      Plus a bad transmission isn’t going to make one cylinder “dead”. I think it has to do with the injector plugs, coil pack or a combination of both. I don’t think it’s a spark plug because they swapped them around. If it were a spark plug then it would’ve followed the plug. The only thing they messed with was the injector plugs and could’ve had a weak coil when it was N/A and ran fine until boost was applied.

  • @bens8696
    @bens8696 11 หลายเดือนก่อน +2

    Rewatched and saw you addressed most of that stuff I guess the only thing might be a worn seat lifter holding the valve open a bit when pumped up but not at low rpm?

  • @sstevocamaro
    @sstevocamaro 11 หลายเดือนก่อน +2

    @1:48 I don’t see any intake runner gaskets..

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +1

      intake gaskets on the Lo Ram are orings in the mating flange

  • @shane-222
    @shane-222 11 หลายเดือนก่อน +3

    Nimble like a ninja!! 🥷

  • @LuisSanchez-nq1sr
    @LuisSanchez-nq1sr 3 หลายเดือนก่อน +3

    So silly question, what DID end up being the issue?

    • @VooDooV6
      @VooDooV6 4 วันที่ผ่านมา

      Also interested..

  • @bensollman8882
    @bensollman8882 10 หลายเดือนก่อน +1

    Tight converter a possibility?

  • @kingsupra5023
    @kingsupra5023 11 หลายเดือนก่อน +2

    What is the best air cold intake for yukon 5.3 2008
    Volant or S&b or k&n or.........?
    Thanks

  • @jasonwilkinson726
    @jasonwilkinson726 11 หลายเดือนก่อน +3

    Check the gasket on the intake to the head on that cylinder

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +1

      no boost leaks-boost was solid

    • @anthonyanderson1479
      @anthonyanderson1479 11 หลายเดือนก่อน

      I dont believe the issue is with the motor

    • @jongoin4404
      @jongoin4404 8 หลายเดือนก่อน

      I think it has to do with the injector plug, coil pack or a combination of both on that particular cylinder. I don’t think it’s a spark plug because you said that you swapped them around, correct? If it were a spark plug and you did move them around then it would’ve followed the plug. The only thing you messed with was the injector plugs and it’s possible that you could’ve had a weak coil when it was N/A and ran fine until boost was applied. 2 months later and have you pinpointed the issue?

  • @baby-sharkgto4902
    @baby-sharkgto4902 11 หลายเดือนก่อน +5

    Sorry if I missed it in the video but what is your cylinder drop test and how did #7 fail said test? Also I think even if one cylinder was down it would still make more power.

    • @nowayjose596
      @nowayjose596 11 หลายเดือนก่อน +4

      A cylinder drop test is more commonly called a power balance test. There are a few different ways to do it but the gist is that, while the engine is running, you deactivate one cylinder at a time by cutting off the fuel and/or spark and seeing what effect that has on the RPM. In a normally operating engine, each cylinder will cause the RPM to drop by the same amount (since they're each equally contributing to the engine running properly). If you have one cylinder that's running poorly and causing your issue, when you deactivate that cylinder the RPM will drop less (or sometimes not at all) compared to the others bc it wasn't contributing as much as the other cylinders were to begin with. So by going through and doing this individually to each cylinder and then comparing them to each other it can help you identify which one is your problem child.

    • @baby-sharkgto4902
      @baby-sharkgto4902 11 หลายเดือนก่อน +1

      @@nowayjose596 thanks for the comment and explanation, I figured that’s what is was. I do them almost everyday I just never knew that there was a term for it. My favorite is to squirt water on the individual exhaust, or check with an infrared temperature gun. Often times guys will pull a plug wire one at a time and *think* that one makes less of a difference and go chasing a problem that doesn’t exist. Probably I might have even done it…… once

    • @nowayjose596
      @nowayjose596 11 หลายเดือนก่อน +1

      @@baby-sharkgto4902 Yeah I was going to ask how he identified #7 was the issue bc looking at the exhaust temp of each cylinder is also an option but then I heard him say they did a drop test. With some scanners (I know you can with Ford's VCM) it can do the power balance test for you and provide a graph of the results without you even having to leave the driver's seat, which is nice. Then there's no confusion about whether or not one cylinder is really dropping the RPM more compared to others like you mentioned.

  • @jasonandjenparks1523
    @jasonandjenparks1523 11 หลายเดือนก่อน +5

    Did you see a dramatic difference in required fuel to get the correct AF ratio? If the one cylinder’s coil was trash, that cylinder would skew the AF lean, which might give you a clue when comparing tunes. Just a guess

    • @lifeishard1211
      @lifeishard1211 11 หลายเดือนก่อน +1

      I just said the same thing, you beat me to it.

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +1

      different injectors

  • @alexmann3309
    @alexmann3309 11 หลายเดือนก่อน +1

    Super soft springs? Or misfiring constantly?

  • @wht240sxka
    @wht240sxka 11 หลายเดือนก่อน +2

    Maybe blowing out the spark, close the gap and run hotter plugs. 3 bar map install. I haven’t followed the full build, but these things plagued me when I’ve built similar projects.

  • @drfeelgood2456
    @drfeelgood2456 10 หลายเดือนก่อน +1

    Id like to put one of these on my 3.5l dodge challenger but i cant find any info on how to do it all mt stock interals are forged so i think it will handle the boost just need to find out how to build the mounting plate

  • @brandonrohrer7914
    @brandonrohrer7914 11 หลายเดือนก่อน +1

    Its that red hose ontop of the supercharger sitting lose boost leak

  • @nowayjose596
    @nowayjose596 11 หลายเดือนก่อน +6

    You already know this but yeah, replacing the coil is the obvious next step. I just replaced one on my truck that was having issues intermittently but just not quite bad enough to actually throw a code.

    • @thatturbotruck
      @thatturbotruck 11 หลายเดือนก่อน +3

      Leakdown test would be my next step before spending any money. If that checks out then coil.

    • @nowayjose596
      @nowayjose596 11 หลายเดือนก่อน +2

      @@thatturbotruck He said they did a compression test and that looked fine, so why would you go on to do a leakdown test in addition to that? Not asking sarcastically, I'm genuinely curious. If you do a power balance test and identify an issue with one cylinder, and then a compression test and that cylinder shows the same compression as the rest, I would move compression to the back of the line as likely culprits and go on to look at fuel and spark. I know a leakdown test can give you more specific information if there IS a problem related to compression, but I can't think of a scenario where it would identify a problem exists (that has been narrowed down to a single cylinder) that a compression test would miss.

    • @thatturbotruck
      @thatturbotruck 11 หลายเดือนก่อน +2

      @@nowayjose596 what you are saying is in general correct. But I've seen these motors have a slightly leaky valve and produce decent compression test results and test bad on a leak down. This is because a small leak may only be down 8-10psi vs the other cylinders which is acceptable yet when it's running and making 1000+psi when compression occurs that small leak becomes much bigger. It's not a guarantee or anything but a test you can run before spending any money is all. I would typically go for compression test first myself.

    • @nowayjose596
      @nowayjose596 11 หลายเดือนก่อน

      @@thatturbotruckThanks for the reply. I agree, if he had a leakdown tester available then while he had the valve cover off would have been an easy time to test that cylinder just to verify.

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +1

      we did a compression test

  • @jtdyalEngineer
    @jtdyalEngineer 11 หลายเดือนก่อน +2

    I can't wait to find out what the source of the problem is... You listed everything I would have possibly checked.

  • @bobbeazley2502
    @bobbeazley2502 11 หลายเดือนก่อน +3

    Welcome to the real world of being a mechanic! Nice job !

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +10

      you would have to welcome me 35 years ago

    • @bobbeazley2502
      @bobbeazley2502 11 หลายเดือนก่อน +1

      I was a GM tech since 1989. Doing the trouble shooting is the worst.

    • @gearjonny369
      @gearjonny369 11 หลายเดือนก่อน +1

      @@richardholdener1727😂

  • @fnafplayer6447
    @fnafplayer6447 11 หลายเดือนก่อน +1

    When will Richard compare that gen 2 lt1 to the ls6 like he said he would which was 2 years ago?

  • @va_innovations
    @va_innovations 11 หลายเดือนก่อน +1

    Keep us updated!

  • @keving2158
    @keving2158 11 หลายเดือนก่อน +1

    I didn't see any intake gaskets when you put the low ram on

  • @sjhudon386
    @sjhudon386 11 หลายเดือนก่อน +1

    Is the trans slipping? I don't think it would still make 7 psi if something was wrong with the motor or the tune.

  • @m97429
    @m97429 11 หลายเดือนก่อน +1

    Exhaust plugged up? Convertor plugged?

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +1

      we dropped the exhaust to check

    • @m97429
      @m97429 11 หลายเดือนก่อน

      @@richardholdener1727 It may seem extreme but you could actually check the exhaust backpressure.

  • @PatKempen
    @PatKempen 11 หลายเดือนก่อน +2

    Looking forward to see what the problem is.
    Could it be the timing chain?

  • @Turbogto_guy
    @Turbogto_guy 11 หลายเดือนก่อน +1

    Did you swap coils with another cylinder? You mentioned injectors and spark plugged being swapped but you didn’t mention swapping coils.

  • @jefft7968
    @jefft7968 11 หลายเดือนก่อน +1

    Did you try turning it off and on again?

  • @jerryvoss3592
    @jerryvoss3592 11 หลายเดือนก่อน +1

    Have you checked out the Comp Turbo oil less center section turbos?

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน

      yes

    • @jerryvoss3592
      @jerryvoss3592 11 หลายเดือนก่อน

      @@richardholdener1727 🤣 Go or no Go? Haven't seen a video from you on them. But, I haven't seen all your vids either:):):)

  • @HGM33021
    @HGM33021 11 หลายเดือนก่อน +1

    maybe that red plug at the back of the intake runner failed and caused a boost leak? or i hate saying it maybe bad tune/ injector timing off?

  • @kingdiesel68
    @kingdiesel68 11 หลายเดือนก่อน +1

    Hey my brother love your videos! We're you able to test pressure in each cylinder? I had seen in the video that the opening is towards the front. I was wondering if the back cylinders were getting as much air? The censors tell the tail! Most people don't have access to a dyno so man do we appreciate what you do!

  • @bntrouble31
    @bntrouble31 9 หลายเดือนก่อน +1

    Coil, collapsing lifter or weak valve spring. One of the 3 for sure..

  • @peterfinley8028
    @peterfinley8028 11 หลายเดือนก่อน +1

    Did you change to colder plugs

  • @larryalexander4833
    @larryalexander4833 11 หลายเดือนก่อน +1

    Dont recall if you said if you ran a compression test and a leak down test or not ? If fuel isnt the issue or spark ?? then compression from piston /rings or valve leaking possible on mechanical side. We know that it isn't timing causeit was running . Also you dont have a major vacum leak on that cylinder? Dont sound like it? Check cylinder pressure

  • @craigdowney6438
    @craigdowney6438 11 หลายเดือนก่อน +1

    On my 02 Saturn, I started getting a "cam sensor" code (the engine doesn't have a cam sensor). I found that the back of the coil pack was corroded and losing ground. I removed it and took some sandpaper to it, and the mating surface on the block. this fixed it for 6 months then it came back and kept returning about every 6 months.

  • @obbyjep7597
    @obbyjep7597 11 หลายเดือนก่อน +3

    Nice truck! We have a 2002 suburban and like it. I wonder if something else is restricting it like the cats having 300000 and flowing enough for stock but not more

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +3

      we tried dropping all the exhaust

    • @bri-manhunter2654
      @bri-manhunter2654 11 หลายเดือนก่อน

      That’s what I was wondering, maybe interment firing could.

    • @obbyjep7597
      @obbyjep7597 11 หลายเดือนก่อน

      I heard that in the talk after, hmm that's a head scratcher. @@richardholdener1727

    • @obbyjep7597
      @obbyjep7597 11 หลายเดือนก่อน

      I'm sure Mr holdener would have looked in wondering how the number7 plug looked after some pulls? Is that low ram intake wanting to work in a rpm range to high? Still would think with 7 psi it would have made more @@richardholdener1727

    • @jackmagnium6115
      @jackmagnium6115 11 หลายเดือนก่อน

      @@richardholdener1727 one of the comments mentions that the cylinder could be bad at RPM and not at idle or off. i think you should rev it out to see what pressures that cylinder is making compared to the rest. i have a bad feeling it could be the valves not seating properly at RPM(and then throw boost into the equation which makes it worse) which is why number 7 could probably be roached

  • @footbraker7070
    @footbraker7070 11 หลายเดือนก่อน +1

    Can’t tell you how many times I have seen them seem to run fine NA, and act up under boost. My latest project was nosing over at 6800, and I tried three different sets of coils before getting good ones.

  • @ObserviantEvolutionaryInnovati
    @ObserviantEvolutionaryInnovati 11 หลายเดือนก่อน +1

    Use a procharger instead? Or Combination of both?

  • @S13KON
    @S13KON 11 หลายเดือนก่อน +1

    What's your cylinder compression numbers ? 😮

  • @jsmiley399
    @jsmiley399 11 หลายเดือนก่อน +1

    Maybe the elbow you have on the supercharger is collapsing like on the engine dyno when you first tried to use the elbow an dthe m90

  • @isaacblankenship1126
    @isaacblankenship1126 10 หลายเดือนก่อน +2

    Im struggling to find a camshaft for my 5.9 magnum that is soon to be a 408 stroker. I have a torque storm supercharger and its in a big truck. Id like to have good torque with a choppy idle.

    • @richardholdener1727
      @richardholdener1727  10 หลายเดือนก่อน +1

      I only see retrofits from Comp that are big enough-maybe another cam manufacturer

  • @ryandoyle4344
    @ryandoyle4344 11 หลายเดือนก่อน +2

    Doesn't sound like unscheduled rapid disassembly

  • @novaracer2000
    @novaracer2000 11 หลายเดือนก่อน +1

    I have a 5.3 in a s10 with a 78/75 vs turbo,sloppy stage 2 cam etc. It also has a #7 missfire and I have changed couls,plugs, wires,injectors and its still there. Sometimes it goes away and then comes back. Very frustrating. I recently pulled the wiring harness and checked it for bad connections and didn't find anything. I am having a issue with water gettung in my gastank that I will be addressing next but not sure that would kill 1 cylinder.

  • @jeremiahs4992
    @jeremiahs4992 11 หลายเดือนก่อน

    Sounded good, and considering you checked just about everything, I wondering if if the Transmission is on the way out the door,

  • @V35Reckless95
    @V35Reckless95 10 หลายเดือนก่อน +1

    Any versions of doing something like this on a 4.6 or a diy turbo setup

    • @richardholdener1727
      @richardholdener1727  10 หลายเดือนก่อน +1

      planned

    • @V35Reckless95
      @V35Reckless95 10 หลายเดือนก่อน

      @richardholdener1727 awesome I can't wait!! Love what you did with the cam battle videos

  • @wfospeedshop
    @wfospeedshop 11 หลายเดือนก่อน +1

    Maybe a MAF disable and a VE tune only would be the way to go. were you maxing out the maf scale with the extra flow? Bc maf takes over at 4k rpm on a factory ecu where you would be making the most power.

  • @Lou_sassel315
    @Lou_sassel315 11 หลายเดือนก่อน +1

    Hello Richard! I have a question about an LS7. I’m getting a decent deal on a complete shortblock LS7 and I already have a set of ls3 heads and intake. Would the heads bolt on and not have any issues with Piston to valve clearance? Or would the different valve angle cause issues like premature valve wear? I don’t want to spend more money for a set of “fixed” LS7 heads and intake when I already have the ls3 stuff! Thank you in advance!

  • @Trucknasty
    @Trucknasty 10 หลายเดือนก่อน +1

    Spark plug gap too wide and blowing out under boost maybe?

  • @calivette805
    @calivette805 11 หลายเดือนก่อน +1

    Good content . Waiting to see what the culprit was

  • @bens8696
    @bens8696 11 หลายเดือนก่อน +1

    Have you tried swapping coils to see if your mis fire moves. Did a small piece of grit get down on the intake valve seat? How many psi boost? Crank pulley same size as one on dyno? Boost leak? Maybe valve seat worn, loosen rocker a bit? That’s all I can think of at the moment ...

    • @lifeishard1211
      @lifeishard1211 11 หลายเดือนก่อน +1

      he did swap coils. he did pull valve covers. boost was at normal levels, I think he said 6lbs.

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน

      I did not do coil swaps yet

    • @lifeishard1211
      @lifeishard1211 11 หลายเดือนก่อน

      @@richardholdener1727 my apologies.

  • @mr.twhosasking5160
    @mr.twhosasking5160 11 หลายเดือนก่อน +1

    Did I miss the intake manifold gaskets? My guess it’s has a major vacuum leak

  • @erickbernard8208
    @erickbernard8208 11 หลายเดือนก่อน +5

    That bronco tho 😂

  • @alexray55
    @alexray55 10 หลายเดือนก่อน +1

    So I was thinking about something and not sure if you've done it or not. But what about a test between holley, edelbrock, maybe carter, and Motorcraft carbs to see what actually makes the most power. Everyone has their own brand they like just like ford, chevy, and dodge people. So instead of comparing engines run all the carbs on one engine no matter what brand engine you choose. Carb ls, sbc BBC, sbf, bbf, small block chrysler, big block chrysler, etc. Think it would be a fun comparison that wouldn't take a lot of work

  • @chandlerlofton6536
    @chandlerlofton6536 11 หลายเดือนก่อน +1

    Cyl leak test. Then drop the y pipe to check for bad cats. Did you swap coil with another hole? I think you said you did. I’ve had a good comp test and still failed leak test. It caused a miss under load.

  • @ricksmash8080
    @ricksmash8080 6 หลายเดือนก่อน +1

    Sorry if this is a stupid question. Is there any way to put an old school hot rod style blower on a 5.3?

  • @r3d1911
    @r3d1911 11 หลายเดือนก่อน +1

    Where are the intake gaskets at on the heads or intake maybe I missed them some place??🤷‍♀️🤷‍♀️🤷‍♀️

  • @christopherc3017
    @christopherc3017 11 หลายเดือนก่อน +1

    Maybe the added pressure is squeezing things to much for plug to ignite past spark. I had a high compression sbc that would kill spark plugs if it didn’t have enough power for the spark.

  • @Sebastianbartledoo
    @Sebastianbartledoo 11 หลายเดือนก่อน +1

    I'd do a re write entire on the tuneup with a charger on it. I've had injectors and o2 sensors go crazy for no reason.

  • @anthonyanderson1479
    @anthonyanderson1479 11 หลายเดือนก่อน +1

    Richard, did Ish have a tune in the trans too? I have dealt with controllers that have a torque map or chart, maybe actual torque exceeded what the trans was compensating for according to map?

    • @anthonyanderson1479
      @anthonyanderson1479 11 หลายเดือนก่อน +1

      Which would cause a slip due to inadaquate line pressure?

    • @anthonyanderson1479
      @anthonyanderson1479 11 หลายเดือนก่อน +1

      Did the trans still have a tps signal? I assume so if you used the stock harness and computer

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน

      tps was hooked up-stock throttle body and harness

  • @ImNotHereToArgueFacts
    @ImNotHereToArgueFacts 11 หลายเดือนก่อน +2

    Did you break a plug/wire with your feet?

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน

      never stepped on that side-but replace that side wire

  • @marksarkaquariums9056
    @marksarkaquariums9056 11 หลายเดือนก่อน +1

    Does the air box flow enough to supply the blower?

  • @70sAirForceBrat
    @70sAirForceBrat 11 หลายเดือนก่อน +6

    I guess at 330,000 mi you don't need to worry about ring gap. It's already self-gapped.

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +5

      that doesn't happen

    • @sons_of_slewfoot_garage
      @sons_of_slewfoot_garage 11 หลายเดือนก่อน

      The lm7 in my turbo s10 had 267k. Went to check ring gap and they were .025-.026 on top and .027 to .028 on the bottom. Slapped em back in and kept the file fit rings for my lh6 lol

    • @70sAirForceBrat
      @70sAirForceBrat 11 หลายเดือนก่อน

      @@sons_of_slewfoot_garage back in the '80s when I did small block overalls used to see excessive ring gap but that was mainly due to cylinder wear I seen up to 0.40 ring gap and seen it worse than that but I said it was due to excessive cylinder wear to where the block had to be 40 to 60 over to clean up because it would have a groove off to one side at the top of the bore. I'm going to be honest I've been out of the game for a long while. Just got back in and everything I seen in pictures and video on the new LS and LT motors. They don't have that issue anymore like the sbc. Thank God. The L59 5.3 with 159,000 on it I picked up when I did the tear down the ring gap was top ring was 0.29 second ring was 0.32 and that was pretty much the same across all the cylinders. That was quite a ring gap for a stock motor with that many miles. The rod and main bearings were perfect! So upgraded to Gen 4 rods and upgraded to summit racing forged pistons raising my CP to 10.6 with 243 heads with a new Z06 camshaft and new cam bearings because I looked at them when everybody said don't.

    • @70sAirForceBrat
      @70sAirForceBrat 11 หลายเดือนก่อน

      @@richardholdener1727 Rich, I based what I said on when I used to work on SBC back in the '80s. Most of what I saw had excessive cylinder wear causing a large ring gap and the cylinders were kind of oval shaped where they had to be bored to 40 to 60 over to clear it up by then the engine at 60 over pretty much junk for a daily driver. But from what I've seen of the newer engines in pictures and videos like you put out in your videos the engines don't have that excessive wear like the sbc did back in the day. I stopped doing engine work in 1987 it went full-time in the car, audio and security business. That's where the money was at that time everybody had to have the boom in their ride. And nobody was going fast with a 1000 to 1500 lb of car audio in their car or truck. LOL The only drag racing I was doing was drag racing but those days are over. My hearing is screwed so it was time for a change of pace.

  • @dantoole9970
    @dantoole9970 11 หลายเดือนก่อน +1

    Compression test the Cyl to make sure it’s up to snuff could have a burnt valve a tuliped valve or a possible ring issue but I would say you might see smoke if the rings were bad.

  • @krichtainswanson1931
    @krichtainswanson1931 3 หลายเดือนก่อน +1

    My thought on this could be wrong but here it is. Seems like a small hole on that plate for all the open area under the supercharger. Also isn't there problems with them getting hot could solve the hot problem by allowing more air through the plate it's mounted to. I could be wrong but seems to be part of boost problem

    • @richardholdener1727
      @richardholdener1727  3 หลายเดือนก่อน

      The opening in the pate is larger than the opening in the bottom of the blower

  • @AndyFromm
    @AndyFromm 11 หลายเดือนก่อน +3

    Sweet bronco!

  • @tytonpurser4430
    @tytonpurser4430 11 หลายเดือนก่อน +1

    Have you ever turbocharged a dodge 5.9 magnum

  • @cockycarguylswayne2211
    @cockycarguylswayne2211 11 หลายเดือนก่อน

    I want to see a big bang video on the aluminum blocks only how much can they really take and what breaks?

  • @lifeishard1211
    @lifeishard1211 11 หลายเดือนก่อน +1

    a couple thoughts, what was the spark plug gap set to? maybe there was spark blowout if the gap was too big. if there was a dead cylinder the air fuel ratio would have been leaner, what was that banks o2 sensor showing? edit for another question, I don't know what setting torque management should be set to for the engine and transmission but that could also be a factor.

  • @michaelkamakaris1640
    @michaelkamakaris1640 11 หลายเดือนก่อน +1

    Possible leak, intake or exhaust side?

  • @roykrossin8343
    @roykrossin8343 11 หลายเดือนก่อน +1

    plastic plug blow out on the intake ? doubt it would take much pressure to do that.

    • @baby-sharkgto4902
      @baby-sharkgto4902 11 หลายเดือนก่อน +1

      I wondered that too at first but he says it’s making 7 lbs

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน

      plug is secured in with a bolt-no boost leaks

  • @tfriesen3866
    @tfriesen3866 11 หลายเดือนก่อน +2

    Try that coil pack. But, you really should have got a NA test before taking it apart for the swap. Time schedule being short, I know, kept you from getting it done before. Two years since the last NA numbers is not that good, if you’re saying the engine has 300k on it.
    You didn’t say if the knock sensors were looked at for pulling timing.

  • @gearratio380
    @gearratio380 11 หลายเดือนก่อน

    i would say just a good tune up and it should be ok, what about knock sensors pulling timing?

  • @bobbywilliams5657
    @bobbywilliams5657 11 หลายเดือนก่อน

    Hi MR Holdener my question is can you use a high performance chip in OEM to adjust tuning

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน +1

      the older chip ECUs could be programmed with timing and fuel changes via changing the chip

  • @frozenstang3868
    @frozenstang3868 11 หลายเดือนก่อน +2

    Do a leak down then move forward from there. Once thats sorted get a pressure gauge on the exhaust ,most likely running into extreme backpressure with a cat that old.

  • @Prestiged_peck
    @Prestiged_peck 11 หลายเดือนก่อน +1

    RICHARD is it possible y'all had a pinhole boost leak on the intake near that cylinder? Im thinking small enough that you'd still make most of the boost, but big enough to throw the AFR for that cylinder rich? Or potentially maybe you had a pre-02 exhaust leak on that bank?
    Also maybe you had a loose connection on that cylinder's injectir during the run, or perhaps that adapter is bad? I do think y'all shouldve swapped that coil before you pullet things apart

  • @9090ruby
    @9090ruby 11 หลายเดือนก่อน +1

    Leak down test?

  • @keithbeauchamp8603
    @keithbeauchamp8603 11 หลายเดือนก่อน +1

    Was there lower intake gasket?

  • @faustthehammer8706
    @faustthehammer8706 11 หลายเดือนก่อน +1

    on the factory 3008 2&3 engines i do belive the mass air fow is in behind the throttle body? its been awhile since i worked on 1 but i think thst part of the reason is youre not pulling enough air past the factory mass air flow? just throwing that out there cause location of that might be part of several issues.

    • @richardholdener1727
      @richardholdener1727  11 หลายเดือนก่อน

      the factory MAF on the truck is in its factory location

  • @EricErnst
    @EricErnst 11 หลายเดือนก่อน +2

    Happy Birthday

  • @coryfuselier3805
    @coryfuselier3805 11 หลายเดือนก่อน +1

    Bad blower actuator? Boost gauge showing boost? 2000 L did the same...

  • @localturbo2969
    @localturbo2969 9 หลายเดือนก่อน +1

    Im planning on doing a m112 on 6 to 7psi should i gap the rings or send it?