MY NEW ESCORT COSWORTH KEEPS OVERHEATING

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  • เผยแพร่เมื่อ 14 ต.ค. 2024
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    The Ford Escort RS Cosworth is a rally version homologation special of the fifth generation European Ford Escort. It was designed to qualify as a Group A car for the World Rally Championship, in which it competed between 1993 and 1998. It was available as a road car from 1992 until 1996. The powertrain was only fitted to this version of the Escort, a longitudinally mounted Cosworth YBT, a highly tunable turbocharged 2.0 L (1,993 cc) with a bore x stroke of 90.8 mm × 77 mm (3.57 in × 3.03 in) Inline-four engine[1][2] which had an output of 227 PS (167 kW; 224 bhp) in standard trim. Tuning companies have achieved power outputs in excess of 1,000 bhp (746 kW; 1,014 PS)

ความคิดเห็น • 432

  • @ramalama9650
    @ramalama9650 11 หลายเดือนก่อน +23

    I can't get over how professional your videos have become. You've done away with that irritating background music and gone straight in with close ups of the work being done. Detailed filming showing your work, good points, mistakes, things to look out for. These videos are good ... VERY good!

  • @mk3escort84
    @mk3escort84 11 หลายเดือนก่อน +38

    Well done mate on the diagnosis. Love watching your work. All the proper checks. Loads of patience . So happy for you finding the issue keep up the good work

  • @theshrew69
    @theshrew69 11 หลายเดือนก่อน +1

    That's a great find not many people would've even looked at that.

  • @tedted5767
    @tedted5767 11 หลายเดือนก่อน +32

    Love the passion you have for these cars. Such a good feeling when you have found fault.

    • @Adam151082
      @Adam151082  11 หลายเดือนก่อน

      Thanks Ted

    • @markcozzie
      @markcozzie 11 หลายเดือนก่อน

      Adam have you seen in the comments someone impersonating you asking them to DM?,just wanted make sure you aware of this??

  • @ahillvfr
    @ahillvfr 11 หลายเดือนก่อน +7

    Before you pull the head off I would check the water jacket parts of the inlet manifold, I used to be a technician @ Ford in the late eighties/early nineties and had quite a few vehicles where the antifreeze had solidified from having too strong a mix and blocked the chambers to the cylinder head from the inlet manifold causing the same sort of fault.

  • @davidhaygarth648
    @davidhaygarth648 11 หลายเดือนก่อน

    Great news ! I would have never suspected that. Saved yourself a fortune.

  • @SecretOfMonkeyIsland784
    @SecretOfMonkeyIsland784 11 หลายเดือนก่อน

    I dont know squat about fixing stuff on cars, but i like Cosworths so this helps me learn a little bit and enjoy seeing a project come together as well

  • @jamesbrannan7449
    @jamesbrannan7449 11 หลายเดือนก่อน +5

    Just goes to show always check the smallest simplest stuff before going to the bigger parts, you do more work but can save so much money, great solve 👍

    • @Adam151082
      @Adam151082  11 หลายเดือนก่อน

      Thanks James

  • @JohnJones-wo1bc
    @JohnJones-wo1bc 11 หลายเดือนก่อน

    Love that car. They were all the rage when I was about 15, and they still look super cool to me! You're a lucky guy to have it!

  • @shaunwilson-seabrook
    @shaunwilson-seabrook 11 หลายเดือนก่อน +7

    Definitely speak to Paul , I’m sure he’d be happy to pass on some advice to help . You could still do the work just be nice to know exactly what the issues are . Great videos . 👍🏻👌🏻👏🏻

  • @edwardboyle808
    @edwardboyle808 11 หลายเดือนก่อน +2

    Adam love the videos interesting informative and definitely fun - reading through the comments posted “try this-do that” stick to the way your doing it with the fault finding, you’ll feel a lot better in your self knowing you’ve done it and solved it yourself… bonus you’ll get to know your baby even more so - you’ll crack it 🔧👍

  • @mickeyflood3808
    @mickeyflood3808 11 หลายเดือนก่อน

    Quality vid. Superb find saved yourself a fortune 🤞🏼 can’t wait for the next video

  • @marklockwood8386
    @marklockwood8386 11 หลายเดือนก่อน

    I only subscribed a few weeks ago I absolutely love your channel not kidding I am 52 and your restoring the cars that we dreamed of in the day its magical

  • @rexim3530
    @rexim3530 11 หลายเดือนก่อน +10

    For the cutting out issue. Open the fuse box and feel for hot relays, most likely fuel pump and then check fuel pump for issues/blockages. Keep up the great work!

    • @markcozzie
      @markcozzie 11 หลายเดือนก่อน +1

      @RealAdamSmithOfficial SCAMMERS

    • @Taz6688
      @Taz6688 11 หลายเดือนก่อน

      Fuel pump relays on Fords were a problem, looking fine, but opening it up you could see the broken trace and burnt board, having said that I'll bet almost every electrical connection will be corroded to some extent, electrical contact cleaner and checking for broken wires,

  • @zoltankerenyi6614
    @zoltankerenyi6614 11 หลายเดือนก่อน +1

    Good job mate! Love your videos and love your Cossie. Wish you a lot of happy miles and twisty corners 😁 Cheers from Hungary!

  • @elliotdavis4641
    @elliotdavis4641 11 หลายเดือนก่อน +6

    Well done mate, hopefully this will sort it. This series is going to be amazing love Escort Cosworth

    • @markcozzie
      @markcozzie 11 หลายเดือนก่อน +1

      @RealAdamSmithOfficial SCAM

  • @mickmiller9936
    @mickmiller9936 11 หลายเดือนก่อน +1

    Perseverance always pays off, well done Adam. Plenty professionals could have misdiagnosed that by not having the patience to cover all bases. You’ll have this mint in no time 👌🏻.

  • @davebrown7527
    @davebrown7527 11 หลายเดือนก่อน +5

    Well done, a lot of people would have had the head off first before realising the banjo bolt was the problem 👍🏻

  • @deejayjay4066
    @deejayjay4066 11 หลายเดือนก่อน +1

    The cutting out issue…..I heard of similar on I believe a Sierra XR4i. Someone had plugged a relay intended for heated rear window into the fuel pump relay position. Hence after so many minutes the car would cut out as the relay timed out. Worth a check if not done already. Thanks for the videos 👍👍

  • @jaredwoodward919
    @jaredwoodward919 11 หลายเดือนก่อน +5

    Good work chap, keeping another cossie legend on the road.

  • @markblacklock588
    @markblacklock588 11 หลายเดือนก่อน

    Well done Adam your persevering is paying off, one job at a time your getting there

  • @RATADATUAVELHA
    @RATADATUAVELHA 11 หลายเดือนก่อน

    great man! love the work and the almost no-editing videos.

  • @andrewonmyway8184
    @andrewonmyway8184 11 หลายเดือนก่อน

    What a great be of investigation. So happy for you you found a cheap fix even though it took time. Great work!

  • @krusher74
    @krusher74 11 หลายเดือนก่อน +6

    its never just that, if that had enough gunk in it to be blocked there is plenty of crap in the rest of the system. it needs a full clean/flush. Use somthing like holts rad flush. The cooling section of the turbo will be partially blocked, you dont want to kill the turbo next.

    • @andyspinks9996
      @andyspinks9996 11 หลายเดือนก่อน

      Good point. Got to be coming from somewhere

  • @johntheman2006
    @johntheman2006 11 หลายเดือนก่อน

    Brilliant. Good thinking testing every part of the system for yourself and well presented.

  • @ascno1970
    @ascno1970 11 หลายเดือนก่อน +1

    well done adam, youre definirely a man who tries & succeeds 🙏🙏👏👏

  • @alanmitchell6302
    @alanmitchell6302 11 หลายเดือนก่อน

    Worth taking your time and checking the basic things first Great work

  • @MaddMattsGarage
    @MaddMattsGarage 11 หลายเดือนก่อน

    Awesome work Adam, late to the party but was saying to the TV check the turbo lines as they suffer the worst metal electrolysis corrosion ever, first time I saw it in person was my 97 Z32 300zx twin turbo engine rebuilding it. However I dig your passion and feel for it, I am reliving my cosworth/max power days vicariously through your videos. Cheers Mate.

  • @the3doorking293
    @the3doorking293 11 หลายเดือนก่อน

    SUPERB CONTENT ADAM.
    Had me in stitches with your comment, "done as much work as a Yummy Mummy from Newcastle" 🤣🤣👍👍👌

  • @kevinmchale6637
    @kevinmchale6637 11 หลายเดือนก่อน

    Well done adam good detective work there pal

  • @TidyRC
    @TidyRC 11 หลายเดือนก่อน

    I’m so thrilled for u mate. Ur dream is still intact 👌🏻👍🏻

  • @TheDickieP
    @TheDickieP 11 หลายเดือนก่อน

    You absolute legend. I’ve been loving this series. I’m on this series ‘like a Geordie on a cossie’

  • @craigdavies9500
    @craigdavies9500 11 หลายเดือนก่อน +1

    I love how you aren't afraid to take things apart Adam. Also love your fault finding skills, Keep on with the cracking videos.

    • @Adam151082
      @Adam151082  11 หลายเดือนก่อน

      Thanks Craig 👍

  • @bishbashbosh-j6z
    @bishbashbosh-j6z 11 หลายเดือนก่อน

    thoroughly well diagnosed, if that's the most you've been into in the engine bay then you're a natural. Engine bay looks well looked after, even coolant reservoir looks new.

  • @johnpells5992
    @johnpells5992 11 หลายเดือนก่อน

    Good job Adam ,great video good luck 👍👍👍

  • @marcuss1754
    @marcuss1754 11 หลายเดือนก่อน

    smashing job mate, absolutely smashed it

  • @garagecedric
    @garagecedric 11 หลายเดือนก่อน +7

    I used these kits which detects exhaust in the coolant, with a blue fluid. Worked for me to find a leaking head gasket, less fun that the engine block wasnt flat enough to keep boost in there. Hopefully it works now though:)

  • @TheVeiledSecret
    @TheVeiledSecret 11 หลายเดือนก่อน +1

    Hello Adam
    From what you describe as the car driving for a very short time ie 5mins and simply cutring out i had the exact same problem on an Escort Cosworth i used to own. I was diagnosed as the Crank Postion Sensor and this was replaced to which the problem was immediately rectified .. the air intake sensor was also replaced as well as a minor precaution. Hope you get it sorted soon and resolve the issue 👍

  • @JonnyMack33
    @JonnyMack33 11 หลายเดือนก่อน +1

    that's mad how you worked back like that..good detective work! I'm 42 and never done more than change a tyre but i feel getting a car to fix now haha! I've learnt that there should usually be fluids, so try air!

  • @matthewlock5833
    @matthewlock5833 11 หลายเดือนก่อน

    A rusty banjo bolt would have been my last guess. Top Work.

  • @hutchy1111
    @hutchy1111 11 หลายเดือนก่อน

    Nice one Adam. Hope the 3 door isn’t getting jealous! We still need some content on the 3 door 👍

  • @c111prs
    @c111prs 11 หลายเดือนก่อน

    What a guy, what a find , I’ve a new fuel pump loom and relays to fit Adam ,,.so when your ready pal ;) one might help your engine cutting out problems, but even if not ,,still a decent upgrade not just a parts chuck

  • @seanhammond4527
    @seanhammond4527 11 หลายเดือนก่อน

    Glad you have found it Adam that’s one of the list of the to do list 😊

  • @tbdogfosters
    @tbdogfosters 11 หลายเดือนก่อน

    great diagnostic mate glad you found the problem 👍

  • @ade-1772
    @ade-1772 11 หลายเดือนก่อน

    nice work and havent seen the end but i would say you have solved the problem

  • @andrewswinglehurst8102
    @andrewswinglehurst8102 11 หลายเดือนก่อน

    Cracking work on a absolute belter of a car

  • @slinkyboy777
    @slinkyboy777 10 หลายเดือนก่อน

    Mint car Adam looks super clean and nicely diagnosed 👍

  • @simonnorcliffe5877
    @simonnorcliffe5877 11 หลายเดือนก่อน

    You are so good with cars , a headgasket 😊is a stroll in the park for you to repair 😮😊😊

  • @chisharpe3304
    @chisharpe3304 11 หลายเดือนก่อน +1

    well done for going through all of these items. Old cars are a bastard sometimes. thanks for the update been waiting to know what it was.

  • @stevo5222
    @stevo5222 11 หลายเดือนก่อน +3

    I'd change the crank sensor as already mentioned, not that expensive and was the fault on mine.
    The fuel filter if blocked can cause the hose to be sucked flat starving the fuel system. That also happened on mine when the car was 2 weeks old!

    • @c111prs
      @c111prs 11 หลายเดือนก่อน

      They always ask when was fuel filter last changed before you go on most dynos , again a good call to change this item ,, that might not fix issues but certainly worth doing

  • @MrMikeyc10
    @MrMikeyc10 11 หลายเดือนก่อน

    Love little fixes like this. So satisfying when you solve something.

  • @hongkongstuey
    @hongkongstuey 11 หลายเดือนก่อน

    I'd have never have guessed turbo banjo bolt!!! Great find, fingers crossed it gets simpler now.

  • @Allenpatch
    @Allenpatch 11 หลายเดือนก่อน

    Well done and a penny chew for your methodical preserverance👍👍👍

  • @adamweston4152
    @adamweston4152 11 หลายเดือนก่อน +4

    I had a escort estate mk3 years ago and it would run for a few minutes and cut out and eventually found out that the crankcase breather pipe was blocked and after cleaning it out it solved the issue and ran fine so maybe have a look at yours Adam, I know it's a longshot but worth a look.

  • @stilostan-the1st
    @stilostan-the1st 11 หลายเดือนก่อน

    You look soooo happy to be working on the escort Cossie, I would be too if it was my own car, good luck sorting out the coolant system

  • @Coolbreeze6132
    @Coolbreeze6132 11 หลายเดือนก่อน

    Nice work mate! Another issue fixed. Looking forward to seeing you take it for a proper run

  • @TezlaByte
    @TezlaByte 11 หลายเดือนก่อน

    Thank you for the update. I'm thrilled to see such a "huge" problem being solved by so little :D I was cheering inside! :D
    And thank you for the more "explain it like I'm 5" :D
    I really like it. A little hard to keep up with your accent some times 😅😅
    Greetings from Denmark

  • @Audifans555
    @Audifans555 11 หลายเดือนก่อน

    Great diagnosis

  • @darrenrevill8664
    @darrenrevill8664 11 หลายเดือนก่อน

    Nice job there. Good to see your doing your homework and not just throwing parts at it. Try a different furl pump relay. My mate had a Sierra with a similar problem. Ended up being that the relay had gone before and he grabbed a spare knocking about. This ended up being a timed heated window relay !

  • @Jay-zq3sy
    @Jay-zq3sy 11 หลายเดือนก่อน

    Some proper fault finding that good job mate

  • @stefmarr
    @stefmarr 11 หลายเดือนก่อน

    Love these vids Adam. Great work

  • @paulriggers1558
    @paulriggers1558 11 หลายเดือนก่อน

    the weak link on escorts of that era were the fuse- boxes, the printed circuit used to burn out around the fuses + relays. i replaced loads in the day, but i wasn't a RS dealer, so didn't do any cossys

  • @staffordshirebullterrierli7411
    @staffordshirebullterrierli7411 11 หลายเดือนก่อน

    That red marker on your 13mm spanner is a good idea mate, Ive always used black pvc tape on my 10, 13, 15 and 17mm sockets 😀

  • @melwebb8485
    @melwebb8485 11 หลายเดือนก่อน

    Good diagnosis also you learn about your car as you go along.

  • @revveduprides5125
    @revveduprides5125 11 หลายเดือนก่อน

    Fantastic vid. Makes a lot of sense what you did there. I’ve got the same problem on my 3dr and the bolt was the only thing I didn’t check. I know what I’m doing this weekend and it’s thanks to you. Awesome and look forward to seeing the next update

  • @garethgriffiths8605
    @garethgriffiths8605 11 หลายเดือนก่อน

    Great work Adam , keep it up.just donated not much but hope it helps , cheeRS 👍

  • @Dalamain
    @Dalamain 11 หลายเดือนก่อน

    New to the channel, I really like the way you make the videos feel like we are there with you fixing the problem, nice job mate - subbed!

  • @mrfizeg8661
    @mrfizeg8661 11 หลายเดือนก่อน

    Well done chap. It will soon be singing away on the roads.

  • @johnmccarthykarting
    @johnmccarthykarting 11 หลายเดือนก่อน

    Can't beat a fast ford your a clever lad love the Cossie content

  • @tricksmoke
    @tricksmoke 11 หลายเดือนก่อน

    Good investigating Adam, for the cutting out issue there is a Guy up your way who has a business called intelligent Auto, he'll sort it .

  • @CreativeHuckleBerry
    @CreativeHuckleBerry 11 หลายเดือนก่อน

    Well done finding that problem, can't wait for the next video 🙂

  • @Se7en983
    @Se7en983 11 หลายเดือนก่อน

    Good work make can wait to see her running properly

  • @robsmith7430
    @robsmith7430 11 หลายเดือนก่อน

    Well done adam that’s a very satisfying video to watch, it will be interesting to see why she’s cutting out

  • @mfordy1056
    @mfordy1056 11 หลายเดือนก่อน

    Good work tracking down the problem. You must be used to the taste of anti freeze by now though……some fittings for your airline next time perhaps. Good luck with the car.

  • @manolisconstantinou8789
    @manolisconstantinou8789 11 หลายเดือนก่อน +1

    Big Paul had sold him this car so he can work on it himself and create content with it . Defeats the object if he gets help from the outsides. Advice is all he might recieve

  • @dannsmcshane1233
    @dannsmcshane1233 11 หลายเดือนก่อน

    Cracking video love your enthusiasm

  • @mark2too
    @mark2too 11 หลายเดือนก่อน

    Superb Adam, step by step diagnosis, until you found the issue! Standing disease is a car's worst enemy.

  • @NathanHiley
    @NathanHiley 11 หลายเดือนก่อน

    Brilliant video Adam and proper diagnosing 💪🏻

  • @alanchurchill7305
    @alanchurchill7305 11 หลายเดือนก่อน +2

    Brilliant deduction Adam great that everything was accessible,hope it sorts it for you mate ,your working through the problems one by one ,it will soon be on the road, wishing you all the best.

    • @Adam151082
      @Adam151082  11 หลายเดือนก่อน +1

      Cheers Alan

  • @kyrienthomas1728
    @kyrienthomas1728 11 หลายเดือนก่อน

    Great job mate happy you got it sorted you needed some look on your side

  • @stevenbutler2030
    @stevenbutler2030 11 หลายเดือนก่อน

    Job well done mate keep going forward

  • @TheGaryprice
    @TheGaryprice 11 หลายเดือนก่อน

    Brilliant video Adam, hats off to you for having a go at this your self.👌🏻

  • @WhildeAutomotiveLTD
    @WhildeAutomotiveLTD 11 หลายเดือนก่อน

    Nice work on this video love the content keep going buddy 🎉👍🏼

  • @sandall1491
    @sandall1491 11 หลายเดือนก่อน

    The joy of when you find the problem, we have all been there 😊. Great vid as usual 👍🤝👏

  • @pauldyer2734
    @pauldyer2734 11 หลายเดือนก่อน

    Great find , all the best on getting her running ! 👍

  • @neildonaldsonlotusexcelresto
    @neildonaldsonlotusexcelresto 11 หลายเดือนก่อน

    Well done Adam... I thought the fact that the expansion tank level was not going down pointed to a blockage rather than the cylinder head gasket....

  • @sxrory
    @sxrory 11 หลายเดือนก่อน

    Always the last hose you check 😂🙄. Lovely car congrats

  • @leekindell9937
    @leekindell9937 11 หลายเดือนก่อน

    Nice work finding it. Looking forward to next update

  • @blueonblueracingnova
    @blueonblueracingnova 11 หลายเดือนก่อน

    The best way to check a radiator isn't blocked is to the the car run up to temp and feel the rad all over to make sure there is no cold spots , filling it with water means nothing it could be half blocked and would still flow water from a hose pipe fine . I wouldn't be too worried even if it was the head gasket its a £200 job at most if your doing it your self . at least its hopefully sorted now though and another job ticked off the list

  • @HollandAmerica-x1t
    @HollandAmerica-x1t 11 หลายเดือนก่อน

    your timing belt also looks like it needs replacement. you can tell by the stripe markings in line with the teeth I would have replaced that.
    and well it is so incredibly easy to swap those belts but you need to do it the correct way and that is also not difficult whatsoever
    great repair by the way
    cheers you got a great car

  • @johnpaulwray4121
    @johnpaulwray4121 11 หลายเดือนก่อน

    Well done on the fault findeing mate great content again keeo them coming

  • @ricksworkshop748
    @ricksworkshop748 11 หลายเดือนก่อน +1

    Have you checked the thermostat? Standing 6 years it can easily be stuck. Test it in boiling water. The turbo pipe would not stop flow through the radiator so i recon when you removed the stat you knocked it enough to free it off. I used to be a Ford RS tech. 🙂

  • @bowmosexual
    @bowmosexual 11 หลายเดือนก่อน

    Great watching you dood, looking forward to the nest one!

  • @mickyhamer1300
    @mickyhamer1300 11 หลายเดือนก่อน

    Love the way you worked through the problem....keep going...you will Win!

  • @racer9877
    @racer9877 11 หลายเดือนก่อน

    Good progress Adam, but get someone to buy you a funnel for Christmas for filling your header tank! 😉

  • @Iusedtobeasweetboy
    @Iusedtobeasweetboy 11 หลายเดือนก่อน

    Always look forward to watching your vids mate

  • @ritchieschofield1185
    @ritchieschofield1185 11 หลายเดือนก่อน

    Nice find that. Lovely car

  • @philfg1
    @philfg1 11 หลายเดือนก่อน

    Great video Adam.
    Less jokes about us Geordies though 😂 hows the championship.

  • @philipbales4921
    @philipbales4921 11 หลายเดือนก่อน

    Adam Smith I admire your confidence in attempting all these things yourself saves a fortune in garage bills...I own a LE 500 E92 M3 DCT and wouldn't dare touch anything under the bonnet 😉 respect to you 👍

  • @brentleajunction
    @brentleajunction 11 หลายเดือนก่อน +3

    Good luck with the car Adam hope this has sorted out the heating on the car onwards and upwards mate