Nomis COP Kit for Khaki!

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  • เผยแพร่เมื่อ 7 พ.ค. 2023
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ความคิดเห็น • 130

  • @nicholasmacausland
    @nicholasmacausland ปีที่แล้ว +13

    Try a cylinder leak down test first in case you don’t see anything by eye so you can know with the numbers you have from the test if it has a issue. If you don’t see anything wrong with the test then it wouldn’t be a mechanical problem with the valve train or the lower rotating assembly sealing wise (rings)

  • @patrickcandler1330
    @patrickcandler1330 ปีที่แล้ว +3

    Glad u grounded that with a regular bolt. I put dress up bolts on mine like that and it made it run funny. So I swapped the one for a regular bolt and bam! Coil on plug gang!

  • @IDABAYAREA650I
    @IDABAYAREA650I ปีที่แล้ว +6

    *Not gonna lie that outro was 🔥🔥*

  • @pascallavoie8434
    @pascallavoie8434 ปีที่แล้ว +12

    Just in time for my weekly dose of DBG

  • @rustyshackleford2525
    @rustyshackleford2525 ปีที่แล้ว +1

    It's the aftermarket fuel rail. I would run OEM injectors and rail. Even the breather bolt for the fuel line.

  • @jeremyellis7364
    @jeremyellis7364 ปีที่แล้ว +4

    Love the outro shot of the db garage door closing at the end. I’ve been watching for a few years now and your editing is getting 🔥

  • @mr.nobody7601
    @mr.nobody7601 ปีที่แล้ว +6

    As was stated by myself and others in a previous video, you have NOT eliminated the distributor being the issue by going COP. It is still using the pick ups inside the distributor that cause the issue. The only way you eliminate that is by using a cam trigger setup like the T1 trigger kit to FULLY eliminate the distributor all together. Didn't it run better on the distributor from JR?

  • @thenotoriouslex7028
    @thenotoriouslex7028 ปีที่แล้ว +1

    ENDING = GANGSTER AF

  • @andrewtoor9898
    @andrewtoor9898 ปีที่แล้ว +2

    Check to make sure your getting your full 14v from the alternator I had a simalar issue on my prelude because my alternator was only putting out 12v

  • @Fackler91
    @Fackler91 ปีที่แล้ว +9

    Check the intake. See if the bolts are tight

    • @VTECgoesBOOM
      @VTECgoesBOOM ปีที่แล้ว +3

      I had thermal intake manifold gasket on my daily, after a year it started getting a funny idle. Manifold bolts ended up coming loose.

    • @2STATICEJ1
      @2STATICEJ1 ปีที่แล้ว +2

      Extended Mani Studs will fix that problem

  • @willmatic84
    @willmatic84 ปีที่แล้ว +3

    Nomis is the man 💪🏽

  • @ronnieprescott6039
    @ronnieprescott6039 ปีที่แล้ว +3

    Vacuum Leak!!!!! Pull your intake manifold

  • @bradleeclark2309
    @bradleeclark2309 ปีที่แล้ว +3

    The only TH-cam channel I get excited about, jeep up the great work

  • @TheModAddict
    @TheModAddict ปีที่แล้ว +4

    Have you changed out the TPS? I dont recall. I had a issue where my TPS was showing 2% duty full closed at idle.
    Also have you quadruple checked vacuum leaks?

  • @skullface9082
    @skullface9082 ปีที่แล้ว +2

    Try a valve lash adjustment before you take off the head

  • @DrivenFilmsPhotography
    @DrivenFilmsPhotography ปีที่แล้ว +5

    Dude its awesome to see it running on COP. I did have one issue with my h accord where it spuddered at around 4k and all i did was unplug the tps and plug it back in and it ran smooth after that. This was after trying to retune it and all

  • @Ondamon375
    @Ondamon375 ปีที่แล้ว +1

    I've been following drivenfilm for a long time from my accord days

  • @abrahamsingleton4681
    @abrahamsingleton4681 ปีที่แล้ว +3

    I want to know what’s wrong now too. It’s got me waiting for the next episode of Khaki like a prime time TV show.

  • @barzaization
    @barzaization ปีที่แล้ว

    Before tearing down a look at the vct solinoid see if it's blocked and if you can find a way to log oil pressure helps

  • @dubiousf00d
    @dubiousf00d ปีที่แล้ว +1

    Now my Monday is complete!🔥🔥

  • @mastercricket7626
    @mastercricket7626 ปีที่แล้ว +5

    The only time the term COP is cool in the street race world 😂.peace and love brotha keep it rad stay safe and build on l8z famz #DBFamStrong #BuiltNotBought #WhoopWhoop

  • @TheHondaHub402
    @TheHondaHub402 ปีที่แล้ว +1

    I would also run a t1 trigger. Cause I believe rn the dizzy is still being used for the stock trigger pickup. So if the trigger is the issue to begin with the cop prob hasn’t fully eliminated that yet.

  • @VTECgoesBOOM
    @VTECgoesBOOM ปีที่แล้ว +4

    Have you done a valve adjust?

  • @chylodavis7573
    @chylodavis7573 ปีที่แล้ว +2

    I think have curly check everything again now that stuff is fresh. Not the tune but it has to be in the data

  • @JSantos777k
    @JSantos777k ปีที่แล้ว +1

    Heck yea!! Great vid! Keep up the edits 👍🏻👍🏻

  • @jairog.3607
    @jairog.3607 ปีที่แล้ว

    Also try to get cam gears as close to stock alignment had them be off by a tooth and little drop of locktite on screws

  • @ChapaRacing
    @ChapaRacing ปีที่แล้ว +1

    I would try to eliminate the fuel filter you have on there make sure the microns are not too high and restricting fuel. Just run the pump direct with no filter and see if that changes anything.

  • @pandamike209
    @pandamike209 ปีที่แล้ว

    Always double check dizzy part in middle shaft for play

  • @codyhenault4597
    @codyhenault4597 ปีที่แล้ว

    Hell yeah fav part of my Monday

  • @kaybevang536
    @kaybevang536 ปีที่แล้ว

    Can’t wait to see the truck be done too shoulda painted the S 10 khaki color 😏

  • @bradleeclark2309
    @bradleeclark2309 ปีที่แล้ว +1

    Maybe a full engine refresh?

  • @sleeperworksgarage
    @sleeperworksgarage ปีที่แล้ว

    Before you pull the head, at least check the valve adjustment. Compression was good so the valves shouldn't be leaking but if they're too tight it'll run rough because there isn't enough air flowing in.

  • @amoralgarage
    @amoralgarage ปีที่แล้ว +1

    Check the voltage on the tps before taking the head off

  • @gregford88
    @gregford88 ปีที่แล้ว

    Do a leak down test before you pull it and check valve adjustment

  • @johnwykoff3256
    @johnwykoff3256 ปีที่แล้ว +1

    I think it is the timing. It might be off. Check your marks on the engine make sure everything is lined up

  • @anybudz
    @anybudz ปีที่แล้ว

    might be due for another high comp b20v build sometime soon👀

  • @scottearls7340
    @scottearls7340 ปีที่แล้ว

    I have been waiting for you to pull the engine apart for a lil minute now lol. I feel your gonna find your issue when you do

  • @RandomAuto12
    @RandomAuto12 ปีที่แล้ว

    Well if you had the ecu gone through and it’s good plus went COP. then changed injectors and have done a pump and filter cleaning. Have plenty of grounds. Ie trans to body engine to body intake to body. Then it’s has to be mechanical either engine or trans. Idr if you have tried Holding the clutch in to see if there is a difference or not. I once had a trans cause mine to lock up but once unbolted the engine spun free or easy.

  • @christopherkelly9548
    @christopherkelly9548 ปีที่แล้ว

    Air/fuel/spark. You took care of spark. I’d get the fuel dialed in then go from there

  • @Otsp922
    @Otsp922 ปีที่แล้ว

    I’ll definitely use Nomis

  • @loudr7622
    @loudr7622 ปีที่แล้ว

    Had the same issues, turns out it was my valves and valve seals were bad. Recommend doing a valve compression test first

  • @thenotoriouslex7028
    @thenotoriouslex7028 ปีที่แล้ว +3

    SOLAR POWER BATTERY TENDER 20$ AMAZON DON'T BE DUM

  • @justinhuffines7162
    @justinhuffines7162 ปีที่แล้ว

    Awesome bro love your channel

  • @victorwilks88
    @victorwilks88 ปีที่แล้ว

    Yeah buddy😮

  • @AlwaysApproved
    @AlwaysApproved ปีที่แล้ว

    damn nomis a gamer. love that

  • @tctnick4156
    @tctnick4156 ปีที่แล้ว +2

    Most certainly doesnt rule out a bad dizzy.
    Your still useing the sensors inside of it. The most important parts. Crappy sensors will 100$ cause issues. Unless you go digidizzy or t1 cam/crank trigger. You still cant rule out that dizzy.

  • @paulkline1522
    @paulkline1522 ปีที่แล้ว

    I would double check Mechanical timing and valve lash. Make sure your fuel pressure is correct too. Does it sound like the iacv is trying to compensate?

  • @Dc2Pichy
    @Dc2Pichy ปีที่แล้ว +1

    Blessings to everyone n most definitely Respect. 🙏💯💪🔥🔥

  • @Dannyass1233
    @Dannyass1233 ปีที่แล้ว

    If braven still worked at O'Reilly you could of got 3 year warranty battery for under 100 bucks with that employee discount

  • @eurocam.
    @eurocam. ปีที่แล้ว

    I wonder if its a sticky valve messing with you comes back fine on test but is actually sticking lowkey

  • @Boosted4whore
    @Boosted4whore ปีที่แล้ว

    Test for head gasket failure maybe ? my gsr would misfire at idle and at WOT misfire would clear up

  • @lonnieciallela1526
    @lonnieciallela1526 ปีที่แล้ว

    Hey love the energy your hysterical. before you tear it down look for a simple leak by spraying brake kleen or carb clean around the intake and throttle body. If I remember correctly from one of your vids dint you have lower compression in one of the cyl. and like islandhonda said do a leakdown test and compression test that will tell you everything before you pull it apart

  • @true2this
    @true2this ปีที่แล้ว

    Have you done a valve adjustment? I had the same issue on my teg and there was 1 valve alil tight

  • @randylour1975
    @randylour1975 ปีที่แล้ว

    Try valve lashing see if it’s gapped right

  • @iJustDab509
    @iJustDab509 ปีที่แล้ว

    Let’s geet it 😎

  • @lookin_litt5483
    @lookin_litt5483 ปีที่แล้ว

    time for a j series khaki 😁😁

  • @taddgadd
    @taddgadd ปีที่แล้ว

    Maybe try a leak down/ compression test I can't remember if you have done those yet. Check for vacuum leaks around intake Manifold

    • @taddgadd
      @taddgadd ปีที่แล้ว

      Oh and the coil on plug is dope as hell lol

  • @stevemartinez7435
    @stevemartinez7435 ปีที่แล้ว

    Came out really clean bro 👌 -unwanted garage

  • @GarageRats
    @GarageRats ปีที่แล้ว

    I am guessing compression test/leak down was good?

  • @abunaiN1
    @abunaiN1 11 หลายเดือนก่อน

    after the cop conversion you need to retune the ecu ?

  • @Cisc0_K1D
    @Cisc0_K1D ปีที่แล้ว

    Have you checked mechanical timing make sure it's not a tooth off?

  • @tylerneisinger206
    @tylerneisinger206 ปีที่แล้ว

    8:45 i saw that. 😂

  • @thesilvafamily883
    @thesilvafamily883 ปีที่แล้ว

    Do a leak down test that will tell u if a valve is leak or even if headgasket not sealing.. good luck

  • @ozzbalz
    @ozzbalz ปีที่แล้ว +1

    @efnstatic @nomis and DBG is what this world needs 👌🏽🫶🏼🙌🏽

  • @prpapy07
    @prpapy07 ปีที่แล้ว

    Have I missed if the spark plugs been. Checked?

  • @dcjuniorb
    @dcjuniorb ปีที่แล้ว

    🎉🎉🎉

  • @jimhiscott2918
    @jimhiscott2918 ปีที่แล้ว

    You probably already looked however can you see the pick-up inside your fuel cell. Is there any obstruction in there possibly?

  • @user-qw9xv1xx3p
    @user-qw9xv1xx3p ปีที่แล้ว +1

    Clogged fuel filter. Dirty fuel lines. Tps might need to be calibrated..

  • @joeymercado4875
    @joeymercado4875 ปีที่แล้ว

    Does the engine have? Enough grounds

  • @JustinFromThe206
    @JustinFromThe206 ปีที่แล้ว +1

    Yup just give Khaki a once over to freshen the engine up then go from there, Eventually add boost too would make for some killer content. #DBFAM

  • @stevelozano9523
    @stevelozano9523 ปีที่แล้ว

    BTW, how many grounds do you have to the block? Honda's kinda finicky with not enough grounds.

  • @Ckiller95
    @Ckiller95 ปีที่แล้ว

    Do a compression test and leave the radiator cap open to see for possible head gasket I don’t think there’s anything wrong with the head cause last compression test it held pressure so you should be good there, try a smoke test for any possible air leaks, if your running an IAC replace/delete it, check your fuel pressure gauge just in case she’s feeding fuel awkwardly like a voltage drop, power probe every individual wire for any possible shorts or faulty connections, get a camera to check for any heat spots/ damage to the piston/ cylinders that can cause detonation issues, or k swap

  • @DanteMusic_LLC
    @DanteMusic_LLC ปีที่แล้ว

    Please take that clip bracket off of the back of the distributor 😂😂

  • @peterdelaat273
    @peterdelaat273 ปีที่แล้ว

    Still my favourite videos where you work on khaki. I'm sure you'll figure out what's wrong with it, keep at it.
    Also the Nomis products look like quality stuff, gotta check it out

  • @thatguyroute76
    @thatguyroute76 ปีที่แล้ว

    Either your head or harness to the injectors

  • @FinessedIt
    @FinessedIt ปีที่แล้ว

    1. More step into right direction with khaki

  • @cedriccope178
    @cedriccope178 ปีที่แล้ว

    Been a minute since ive seen one of your videos

  • @Runaeh
    @Runaeh ปีที่แล้ว +1

    get a vibrant ultra quiet resonator for it instead, its way to loud...

  • @tommoon2700
    @tommoon2700 ปีที่แล้ว

    #dbfam strong boiiii

  • @LD_Builds
    @LD_Builds ปีที่แล้ว

    Check I ideal air control valve..

  • @anthonyschwemm
    @anthonyschwemm ปีที่แล้ว

    Do a valve adjustment

  • @julianwestmoreland84
    @julianwestmoreland84 ปีที่แล้ว

    🔥🔥🔥🔥🔥💯

  • @natlikethebug9522
    @natlikethebug9522 ปีที่แล้ว

    Maybe your timing is off? I dont remember if you mixed and matched parts (its been a while since the og build since it blew). It could be stuff not working well together or something simple as being a tooth off?

  • @1illlawn192
    @1illlawn192 ปีที่แล้ว

    DB!!🎉

  • @hopkinsgarage8787
    @hopkinsgarage8787 ปีที่แล้ว

    keep pushing on khaki brotha youll find out soon whats wrong #OGDBGF

  • @masterturkey2001
    @masterturkey2001 ปีที่แล้ว

    Open the engine up! Maybe this is what needs to be done. But like I said before. I think the crank jumped a tooth. It happens when ever you down shift hard or money shift. Hopefully you find the issue soon. I have lots of faith on the B series.

  • @Deanowp
    @Deanowp ปีที่แล้ว

    Its a sign to Kswap Khaki

  • @brysonapolo867
    @brysonapolo867 ปีที่แล้ว

    fuel filter clean

  • @timbrowning7272
    @timbrowning7272 ปีที่แล้ว

    Check wiring I've seen it to many time a perfect wired car two wires causing an interface

  • @Fackler91
    @Fackler91 ปีที่แล้ว +1

    That's legit

  • @bonezy2188
    @bonezy2188 ปีที่แล้ว

    Before pulling head , you can do a leak down test forcing air into the cylinder and Ratchet on crack. Check you tube video if u don’t know , ‘. and I think u have done compression test so u good there , Swap out sensors , if have some laying around or junk yard some , air temp ‘ coolant temp etc , also ,
    have u swap out main relay , if. All possible try getting a stock one junk yard or if u have extras not a part store one. Happened to my buddy his went out 2 days later after buying a new one
    Fuel pressure at 55 , On your MAP sensor. If u ever took it off. Make sure the O ring is there U can also take throttle body off and make sure the air port is clear. Living in a dusty area
    Hope we all got to tickle your brain a little. & Hope we all help you get Before pulling the head and acts the same 😂. Stay safe bro !!!

  • @richardjimenezjr5068
    @richardjimenezjr5068 ปีที่แล้ว

    Is your fuel line even big enough

  • @kevinkev1530
    @kevinkev1530 ปีที่แล้ว

    👍🏾👍🏾

  • @carlosfernandes24
    @carlosfernandes24 ปีที่แล้ว +2

    Check your timing

  • @felixcruz974
    @felixcruz974 ปีที่แล้ว

    Mandala pa can en Ohio. I need a new work Truck 😂. TRX gonna be Sweet

  • @JustinFromThe206
    @JustinFromThe206 ปีที่แล้ว

    #DBFAM

  • @2STATICEJ1
    @2STATICEJ1 ปีที่แล้ว

    Check IAC valve

  • @julianwestmoreland84
    @julianwestmoreland84 ปีที่แล้ว

    Yooo

  • @SuperBigNye
    @SuperBigNye ปีที่แล้ว

    do a leak down test before you pull the head

  • @DrDr1v1
    @DrDr1v1 ปีที่แล้ว

    Brooooooo check you tps sensor pls