I Damaged my HKS RB28 Engine in my R34 GTR

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  • เผยแพร่เมื่อ 29 ก.ย. 2024
  • Its a sad day in the shop as we pull apart the RB28 in the GTR. In the last video I showed a clip where I mis shifted and threw a check engine light and limped the GTR back to the shop. Lets figure out what we damaged.

ความคิดเห็น • 905

  • @AdamLZ
    @AdamLZ ปีที่แล้ว +4553

    Granny shifting… not double clutching like you should. Now me and the mad scientist gotta rip apart the block to fix the piston rings you fried. 🤦‍♂️

    • @PositionGain
      @PositionGain ปีที่แล้ว +48

      U funny 😂😂

    • @kellinpatler
      @kellinpatler ปีที่แล้ว +7

      😂😂😂😂

    • @slimsincere5015
      @slimsincere5015 ปีที่แล้ว +7

      😂😂😂 #DomTorrettoVc😂😂😂

    • @EL_P2Though
      @EL_P2Though ปีที่แล้ว +8

      Hell nah 😭😭😂😂

    • @ism7916
      @ism7916 ปีที่แล้ว +74

      I'd say Adam won this comment smack down! lol classic!

  • @lokijones8324
    @lokijones8324 ปีที่แล้ว +9

    Make sure that you check piston to deck height on every piston while you have the head off. If you over revel it, had a blown head gasket, and coolant leak issue, you could have possibly bent a rod, or squished a rod bearing. Good to check now before you slap the head on.

  • @MrMinemadness
    @MrMinemadness ปีที่แล้ว +4

    Sounds like the headstuds weren't retorqued after a some heat cycles to me.

  • @BattlingWarrior1985
    @BattlingWarrior1985 ปีที่แล้ว +2

    So glad it was just the gasket and that you didn't have to buy a whole new head or block

  • @wwilliams1919
    @wwilliams1919 ปีที่แล้ว

    Clearly a head gasket simple replacement 5 hour job and back driving. The head can be easily removed in the engine bay. But i understand the overkill of removing the engine for the dramatic video effect.

  • @Benjii002
    @Benjii002 ปีที่แล้ว

    Ouch, you got lucky man

  • @Rekoyl116
    @Rekoyl116 ปีที่แล้ว

    think about the cylinder pressure created when you money shift. its like engine braking x 100. lucky its a headgasket and you didnt bend a rod, or a valve. fyi youre mean to re-torque the head studs, i dont think theyre stretched i just think theyre loose

  • @ALTF26
    @ALTF26 ปีที่แล้ว +594

    Don’t let any of this distract you from the fact that Hector is going to be running 3 Honda Civics with spoon engines, 3 T66 turbos, with NOS, and a Motec system exhaust.

  • @KingJojoB
    @KingJojoB ปีที่แล้ว +184

    If you didn’t come from tiktok raise your hand 🤚🏽

  • @sputnikalgrim
    @sputnikalgrim ปีที่แล้ว +893

    Leave it to TJ to wait 2 years on a build just to mess it up a week after delivery

    • @jesseortiz9007
      @jesseortiz9007 ปีที่แล้ว +23

      It's comical how easy it is to shift from 2nd gear to 3rd gear in these cars. I honestly laughed when it happened considering how easy it was to shift this car when I drive em.

    • @bg710
      @bg710 ปีที่แล้ว +28

      @@jesseortiz9007 but but but the transmission was cold 🤣🤣

    • @Crazy_CAT16
      @Crazy_CAT16 ปีที่แล้ว +7

      @@bg710 rookie mistake

    • @emilianofajardo9487
      @emilianofajardo9487 ปีที่แล้ว +9

      @@jesseortiz9007yeah but right hand drive is honestly very easy to confuse

    • @jesseortiz9007
      @jesseortiz9007 ปีที่แล้ว +12

      @@emilianofajardo9487 Shift pattern is exactly the same, only thing that changes is what hand you use to shift with. RHD doesn't change the gear pattern

  • @hybridevolve6759
    @hybridevolve6759 ปีที่แล้ว +144

    I know it’s a bad situation. But these in detail videos are the one 👌

  • @TeknicZ
    @TeknicZ ปีที่แล้ว +69

    Didn’t hear you say it but it would be in best interest to also replace those studs if Ian is saying those rear nuts didn’t crack when removing them then it is highly possible that they won’t torque down properly not 100% likely but it’s better safe than sorry

    • @Vitormarques542
      @Vitormarques542 ปีที่แล้ว +7

      probably they werent torqued right from the beginning

    • @toft5320
      @toft5320 ปีที่แล้ว +9

      they are not reusable to begin with and im sure these dudes know that

    • @boboso7238
      @boboso7238 ปีที่แล้ว +7

      Nah bro, the goat went to the goat, spent goat money to get the goat built. No way they missed a torque spec. 🐐🤣🤫

    • @boboso7238
      @boboso7238 ปีที่แล้ว

      @@toft5320 JB weld fixes everything.

    • @TeknicZ
      @TeknicZ ปีที่แล้ว

      @@boboso7238 you ain’t lying I jb welded my drive shaft back together 4 years ago after it split in half and it’s still together vibrates a lot but it drives

  • @David5Suggs
    @David5Suggs ปีที่แล้ว +79

    This is a really painful video, but I appreciate this type of video. You're incredibly open & honest about a shit situation and we appreciate it whole-heartedly. These videos are great none-the-less.

    • @allspooledup2584
      @allspooledup2584 ปีที่แล้ว +1

      Really not that painful at all if it’s just a head gasket. That’s like best case scenario

    • @fredericoespinoza
      @fredericoespinoza ปีที่แล้ว

      its just more content to make more money bro shush

  • @Nick.Pellerin
    @Nick.Pellerin ปีที่แล้ว +50

    7:07 His face followed by Tj's look on his face like "this is not funny" was priceless😂😂

  • @johnnybenefield5030
    @johnnybenefield5030 ปีที่แล้ว +61

    The reason you always take out all the spark plugs to do a compression test is which it should have showed up in your test is if it has a bad spot in-between two cylinders with the plugs in it will not show up but with all plugs out it will 99% of the time

    • @xiukn8
      @xiukn8 ปีที่แล้ว +4

      But compression test was still good 😂

    • @johnnybenefield5030
      @johnnybenefield5030 ปีที่แล้ว +2

      @@xiukn8 that is why I said 99% of the time

    • @duanebailey6253
      @duanebailey6253 ปีที่แล้ว +3

      The valves open and close giving an escape point. Plugs wouldn't really change that. As seen from no variance in both tests.

    • @johnnybenefield5030
      @johnnybenefield5030 ปีที่แล้ว +4

      @@duanebailey6253 I have been working on motors for 30 years and like I said it matters most of the time but like I said not always. It matters how bad the head gasket is blown. TJ's if you look it wasn't bad because he shut it down fast, if he kept running it would have especially when it eats a grove in the gasket.

  • @OGAwsomSauce
    @OGAwsomSauce ปีที่แล้ว +22

    Did you guys see the chipped valve? This kind of gasket blowout is common on 10th Gen civics

    • @MichaelDrowley
      @MichaelDrowley ปีที่แล้ว +3

      Yeah, can’t believe they didn’t see that.

    • @rojo9063
      @rojo9063 ปีที่แล้ว

      Fr

    • @jhall9936
      @jhall9936 ปีที่แล้ว +2

      Came looking for this comment I was like surely they noticed the chipped valve

    • @DriftNick
      @DriftNick ปีที่แล้ว

      It's not chipped, just some crap on the valve.

  • @kylenewberry8598
    @kylenewberry8598 ปีที่แล้ว +34

    Didn't tommy say the headgasket was sketch when he was building anyway?

    • @hawaiian_judge5113
      @hawaiian_judge5113 ปีที่แล้ว +6

      yarrrr

    • @171JUSTIN
      @171JUSTIN ปีที่แล้ว +1

      How so? And why use it if the builder admits it's sketch?

    • @kylenewberry8598
      @kylenewberry8598 ปีที่แล้ว +2

      @@171JUSTIN basically said that by design the gaskets can leak, but they don't usually give problems. But if they do, just replace them, but saves money in the initial build.

    • @Aintchuhurd
      @Aintchuhurd ปีที่แล้ว +13

      Tommy is sketch

    • @Coyoteluvr
      @Coyoteluvr ปีที่แล้ว +4

      That engine was fk from the moment he started it. Ity smoked so much. I think that Tommy might made a mistake.

  • @Steu022
    @Steu022 ปีที่แล้ว +16

    If you remember a few episodes back during the build/tune on the car, you guys had mentioned you noticed a good amount of smoke coming from the tale pipe which could have been the start of the gasket going 🤷‍♂️

  • @kontrix1
    @kontrix1 ปีที่แล้ว +11

    13:20 you have a broken valve as well

    • @kopyking37
      @kopyking37 ปีที่แล้ว

      Saw that too

    • @Crazy_CAT16
      @Crazy_CAT16 ปีที่แล้ว

      it looks like it's the coating on the head gasket

    • @justinchapman5774
      @justinchapman5774 ปีที่แล้ว +1

      Definitely looks like a piece of the valve is missing, definitely look at the valve next to where the head gasket blew, it may just be carbon but even zoomed in on looks broken

    • @DylanTK
      @DylanTK ปีที่แล้ว +1

      yep, and that's exactly what lifted the head

    • @MichaelDrowley
      @MichaelDrowley ปีที่แล้ว

      Yep

  • @gregcass12
    @gregcass12 ปีที่แล้ว +173

    Imagine paying $70k for a motor then money shifting 😂

    • @JoshQc
      @JoshQc ปีที่แล้ว +23

      He payed more than 70k buddy, over 100k

    • @wotceseriescollector
      @wotceseriescollector ปีที่แล้ว +14

      he will keep making vids until it pays for it

    • @loan-shark
      @loan-shark ปีที่แล้ว +30

      he's a millionaire - this is content.. wish i had a staff working on my cars while earning money 😂

    • @boboso7238
      @boboso7238 ปีที่แล้ว +9

      The S2000 has more than $100K under that hood. The Skyline easily has more than that in labor and anodized colored parts, Tommy got to get paaaaiiid.🤣

    • @JDMz
      @JDMz ปีที่แล้ว +4

      ​@@JoshQche paid 100k in just exterior mods let alone the engine 👁👄👁

  • @EpicBurnReturn
    @EpicBurnReturn ปีที่แล้ว +25

    You need to check bearing clearances after money shifting🤑

  • @Lincolnr82
    @Lincolnr82 ปีที่แล้ว +7

    That money shift could have caused an over-boost, lifting the head and torching the head gasket. And of course, like everyone else mentions, make sure to replace the head studs. Seems like you stretched the back ones.

  • @justinchapman5774
    @justinchapman5774 ปีที่แล้ว +37

    Look at the valve next to the blown part of the head gasket, definitely looks like a piece is broken off of it, 13:22

    • @rivalspec1210
      @rivalspec1210 ปีที่แล้ว +3

      Could be just dirt, the compression test would have shown low compression

    • @Crazy_CAT16
      @Crazy_CAT16 ปีที่แล้ว +2

      it's the coating on the head gasket

    • @GramSnax
      @GramSnax ปีที่แล้ว

      solid eyes, that absolutely looks like its potentially chipped

    • @MichaelDrowley
      @MichaelDrowley ปีที่แล้ว

      Also spotted this, The valve is gonskies

    • @Nathan.t140
      @Nathan.t140 ปีที่แล้ว

      Bro it looks like grease of carbon build up

  • @auralxtc
    @auralxtc ปีที่แล้ว +18

    If you get away with just a blown head gasket, you are doing alright. Much better than a bent rod or a valve issue.

    • @duanebailey6253
      @duanebailey6253 ปีที่แล้ว

      I'd be more worried about the crank and bearings. Doesn't take much to upset them early on especially with added rpm/harmonics.

  • @BoostedSpeedDemon
    @BoostedSpeedDemon ปีที่แล้ว +2

    How did nobody notice the big chunk missing out of the valve by the head gasket failure? 13:21

    • @DriftNick
      @DriftNick ปีที่แล้ว

      It's just some crap on the valve.

  • @nickouzounian8415
    @nickouzounian8415 ปีที่แล้ว +36

    Bro I learned so much from this video you guys explained everything so well

  • @chiva4life17
    @chiva4life17 ปีที่แล้ว +3

    Anyone catch that yellow R33 sneak peek at 14:28 lol?

  • @nozzomeister844
    @nozzomeister844 ปีที่แล้ว +2

    Anyone else see the teased R34 GTT left rear quarter in the end of the video when he puts the hand over the camera! New project?!

  • @lIlIllll1
    @lIlIllll1 ปีที่แล้ว +4

    Thats why u can't trust tommy to build shii

    • @kulvircheema955
      @kulvircheema955 ปีที่แล้ว

      I totally agree with you

    • @Crazy_CAT16
      @Crazy_CAT16 ปีที่แล้ว

      That's why Adam's engine setup on the R32 is very different from the build that Tommy usually does, that's what Tommy talks about in his video.

  • @AlexDrifts
    @AlexDrifts ปีที่แล้ว +3

    That is the EXACT area the block fails in Rb blocks, CHECK THE HEAD STUD GOING INTO THE BLOCK!!!! There may be slight cracks showing on side of block.
    if you magnaflux the block you should see it. CHECK THE BLOCK!!!!

  • @cppctek
    @cppctek ปีที่แล้ว +9

    Replace the studs. Replace the gasket. Check the deck surface for any high or low spots not just cracks

    • @thepunisher3810
      @thepunisher3810 ปีที่แล้ว

      Bearing clearances need to be checked amongst other things as well

  • @vickomf1
    @vickomf1 ปีที่แล้ว +6

    I was looking forward to this video YESTERDAY!!!

  • @sarahm3881
    @sarahm3881 ปีที่แล้ว +10

    My Toyota Camry would neverrrr 😂

    • @ND-ICU
      @ND-ICU ปีที่แล้ว

      My Camry Blew the a head gasket first then Blew the Engine a couple months later 😂😂😭😭😭

  • @functiongarage
    @functiongarage ปีที่แล้ว +6

    Leakdown test called it on the last vid. Been through it before. Pressurize it and the air will find a way out. You probably detonated on the over rev it's alot of cylinder pressure. Glad it's only the head gasket I've had much worse outcomes.

  • @iggy_gtr
    @iggy_gtr ปีที่แล้ว +7

    headlift, use the same spec studs. If you use 625 and it was torque plated with 2000s, you'll get really bad wear or scratching in the bore later on

    • @Raceman
      @Raceman ปีที่แล้ว

      why this happends?

    • @iggy_gtr
      @iggy_gtr ปีที่แล้ว +4

      In RB's if you machine a bore to be straight without a torque plate, and clamp the head down, the same bore that was straight prior will start to show distortion. Same issue can happen if you significantly increase clamping load on the RB if it was torque plated with a certain type of headstud. Increasing the clamping force from when it was torque plated with ARP2000 headstuds, to say ARP625, can cause changes in the bore which after some use can be visible scratching in the bore, or unusual wear in the tops of the bore.
      In this situation would be best to get a new set of the same headstuds the motor would have been machined with @@Raceman

  • @2jyeti909
    @2jyeti909 ปีที่แล้ว +4

    So i guess this means adam has the better R34 GTR 😂

  • @Aerospacegod
    @Aerospacegod ปีที่แล้ว +9

    Im kinda shocked that the transmission doesnt have a first gear lockout. Maybe it's a possible change that can be made? I'm not sure at all just throwing it out there.

    • @MrHughk1
      @MrHughk1 ปีที่แล้ว

      Its a manual gearbox, MANUAL ie its not an automatic so no it does not have a first gear lock out. Could it be done with a computer and numatics, of course but then you would just automate the shift fully and you have an automatic gearbox. The point is that it takes a certain level of skill to use the manual and that is part of the attraction to master the fast 1/4 or lap. TJ just fucked up here showing off his huge wallet.

    • @yourdaddy9622
      @yourdaddy9622 ปีที่แล้ว +8

      @@MrHughk1you obviously don’t drive a manual buddy, they have had first and reverse lockouts for almost two decades. Maybe don’t cut someone down when you have no idea what you’re talking about. Having5 or 6 gears and a lock out of 1st doesn’t “basically make it an automatic”, you just don’t have a permit yet so are going off of video games.

    • @MrHughk1
      @MrHughk1 ปีที่แล้ว

      @@yourdaddy9622 Reverse yes, first is pointless even if it has been done as if you do one you need to do all as you are de skilling the driver, which makes it basically half way to being an automatic, only a clutch actuator is then required. Dont be so presumptuous yourself, im 56, got a degree in mechanical eng and work on cars and bikes for fun. And remember we are talking about early 90's tech before people catered for the lowest achiever at the expense of everyone else. Getting an award just for turning up breeds idiots like you and the commenter.

    • @duanebailey6253
      @duanebailey6253 ปีที่แล้ว

      ​@@yourdaddy9622normally done on the shifter. It's a pain in the butt for a street car though.

    • @yourdaddy9622
      @yourdaddy9622 ปีที่แล้ว

      @@duanebailey6253 like as much of a pain as literally changing every bolt on the car? You know, like he did with Tommy… yikes

  • @B_M_A
    @B_M_A ปีที่แล้ว +37

    That's super weird that it blew the gasket. I wasn't expecting that purely because it's not common considering the circumstances. Must just be how the motor is spec'd out.

    • @slabgizor1176
      @slabgizor1176 ปีที่แล้ว

      I suppose because it lifted the head

    • @estebanquito356
      @estebanquito356 ปีที่แล้ว

      Exaclty, that engine most probably had bad timing due to the over rev, then it blew the head gasket. With only the head gasket blown it can still rev up and run, even the first compression test was ok so the car should still run. Also you can hear it miss firing evenly not only 2 cylinders.

    • @25Neo
      @25Neo ปีที่แล้ว

      its actually a very common thing to happen when a head is lifted, especially considering the motor was over revved, its not like lifting a head from to much boost or not good enough head studs, as well as the head being lifted, there is so much combustion at 10-11k rpm or whatever rpm it may have revved out to, im surprised it didnt blow the head gasket worse

    • @duanebailey6253
      @duanebailey6253 ปีที่แล้ว +1

      This is why you always check the studs after the break in period. Things change after a few heat cycles. But even still the added harmonics from the over rev will be enough to damage things. These blocks have no bracing at all. The spoon ceo breaks it down well comparing blocks. Think it's when they rev the b16 over 11k.

  • @wbass243
    @wbass243 ปีที่แล้ว +5

    TJ, Also get the replacement parts that you need when you do maintenance, like main seals and any other seals that need to be flown in from Japan. You can cover each part with vasoline (assuming they are ok to be contacted with petrol )and vacuum seal them with a vacuum seal bag. then when its time to use them degrease them and clean them nicely so you have the parts on hand. Keep them away from sunlight and oxygen and they should last 10 years

  • @mj_aussie_coaster_travels8310
    @mj_aussie_coaster_travels8310 ปีที่แล้ว +2

    My moneys on that head gasket being poo since day one. The mis shift just nailed it.
    When the builder says the gaskets are crap and doesn’t replace it with a trusted brand to keep costs down on a half million dollar Datsun there’s something not quite right.

  • @halfbloodentertainment
    @halfbloodentertainment ปีที่แล้ว +13

    Woah what happened ? Didn’t I watch this yesterday 🤣 either way, poor FineSpec😭 we praying for y’all🙏🏼

    • @adamportman9084
      @adamportman9084 ปีที่แล้ว

      i was triple out

    • @adamportman9084
      @adamportman9084 ปีที่แล้ว

      trippin

    • @MrSelmo85
      @MrSelmo85 ปีที่แล้ว +3

      When i tried to watch it yesterday it was set to private.. something was likley cut..

  • @BCs300z
    @BCs300z ปีที่แล้ว +1

    bro! the oil splash covers in the head, over the cams, are in an RB25 configuration.... not the correct RB26 configuration for the valve covers and baffles.

  • @rozijntje
    @rozijntje ปีที่แล้ว +9

    Check the valves for seal, the most common result of misshifting is actually valves touching the pistons due to very high rpms at that point.
    You might have bent a valve or two.

    • @fabini14
      @fabini14 ปีที่แล้ว

      Leak down test is good impossible to have bent valves.

    • @slabgizor1176
      @slabgizor1176 ปีที่แล้ว

      They would've known when they did a second compression test

    • @jonathanclarke452
      @jonathanclarke452 ปีที่แล้ว +3

      13:20 shows a broken valve

    • @fabini14
      @fabini14 ปีที่แล้ว

      @@jonathanclarke452You are wrong lol is just carbon on top of the valve... they have done leak down is impossible to have bad valves

    • @jonathanclarke452
      @jonathanclarke452 ปีที่แล้ว

      @@fabini14 lol? Chill with the big brain attitude. It might be but there’s a lighter colour gold in the crease where I think the crack is. I didn’t see the compression test so it’s just off their word. Wouldn’t doubt them trying to sell parts and be less than forthcoming about their condition publicly. Could have just been overlooked in editing. My engine has better compression numbers than this but bad leak down. Still drives fine and have run it like that for years now.

  • @johnjoseph3908
    @johnjoseph3908 ปีที่แล้ว +4

    not gonna lie. tj u scored big time with bringing Ethan to the team. mans a automotive monster.

  • @juddy953
    @juddy953 ปีที่แล้ว +1

    Tj u NEED to call the AUSSIES to build u a proper engine. Getting the zinc bolt on can guy was the worst decision u have made

  • @spliff08
    @spliff08 ปีที่แล้ว +6

    TJ bricked his $100,000 car 😂

    • @deanwilson9317
      @deanwilson9317 ปีที่แล้ว +4

      If I had to guess $100,000 is an understatement…

    • @drewole
      @drewole ปีที่แล้ว +1

      Bro, thats worth way more than 100k

    • @connoisseuroftigolbitts
      @connoisseuroftigolbitts ปีที่แล้ว +1

      Try more like $250k +

    • @johnathanromero3944
      @johnathanromero3944 ปีที่แล้ว +2

      He could brick a $5 car or a $1,000,000 car… it’s TJ, he’s got ZERO clues about cars and it shows in every video…. One of the reasons I watch it is to get a laugh at someone “so accomplished” in racing and cars knows absolutely NOTHING about cars and can only read a script and not a repair manual…. Sad

  • @KableTac
    @KableTac ปีที่แล้ว +2

    pretty standard feature for every tommy spec engine.

  • @martinellis3327
    @martinellis3327 ปีที่แล้ว +5

    I really enjoyed and appreciated you guys brainstorming and explaining what it was you were doing and seeing, from someone who loves cars but has limited mechanical knowledge, it was great!

  • @TheTrifectaDeroMan
    @TheTrifectaDeroMan ปีที่แล้ว +1

    Sounds like typical work from fyeah... He only used 20% of the parts so as soon as it saw high revs the coils dildo'd the engine

  • @Dirtyz1234
    @Dirtyz1234 ปีที่แล้ว +3

    Did you even hose the gasket down with copper spray and say "that ain't goin nowhere" 😅

  • @erichernandez1110
    @erichernandez1110 ปีที่แล้ว +3

    Hopefully its back up soon! Get a straight edge and feeler gauge to check the flatness of the decks, too far gone would just cook the new head gasket.

  • @duanebailey6253
    @duanebailey6253 ปีที่แล้ว +1

    Check the oil. Sounds like a spun bearing. It will go away and come back. Engine didnt sound right and knocking in certain points.

  • @chrissantana6688
    @chrissantana6688 ปีที่แล้ว +5

    why'd you take down the video from yesterday, did you not want people to see the yellow r34 in the background that may be the next giveaway car or that tommy is coming down to help and do another project?

    • @ColinRay999
      @ColinRay999 ปีที่แล้ว

      Awfully specific comment lol

  • @XoliQCX
    @XoliQCX ปีที่แล้ว +1

    If you look at 13:26 there is what is looking like a burnt/broken exhaust valve

  • @Jyuaa
    @Jyuaa ปีที่แล้ว +3

    Hey TJ hope everything goes well brother 👍🏽

  • @phosimmie
    @phosimmie ปีที่แล้ว +2

    Who else was able to watch yesterday? Noti Gang!

  • @dennnster
    @dennnster ปีที่แล้ว +6

    Hi TJ. So when are you getting a NSX? ;) Love the content!!

  • @__jacob
    @__jacob ปีที่แล้ว +2

    YELLOW R34?! I see you

  • @johnathanromero3944
    @johnathanromero3944 ปีที่แล้ว +22

    Blows my mind just how little TJ knows about cars…. Truly mind blowing! 🤦🏼‍♂️

    • @wotceseriescollector
      @wotceseriescollector ปีที่แล้ว +3

      agreed

    • @2jyeti909
      @2jyeti909 ปีที่แล้ว +11

      Could be worse. Could be DDE.

    • @SUp3RpooP3r7698
      @SUp3RpooP3r7698 ปีที่แล้ว +4

      Well, I mean these guys aren't mechanics. They're TH-camrs with money. I mean, I'm sure they know their fair share. But that's why they hire other people to work on their cars

    • @Justinhomii
      @Justinhomii ปีที่แล้ว

      Too busy putting rivets in widebody's to learn about engines

    • @chrisdef15
      @chrisdef15 ปีที่แล้ว +1

      What did you expect? As others said he’s a youtuber. But from your comment he still probably knows more than you. You just criticised without giving any advice.
      2 guys who do know. 3 if you count tommy took a while to figure it out. But I’m sure you know more.

  • @BlakesGarage
    @BlakesGarage ปีที่แล้ว +1

    Bro 13:25 that valve looks like it’s missing a chunk out of it.

    • @Bruce_Wesley
      @Bruce_Wesley ปีที่แล้ว +1

      I saw the same thing at 13:09. Glad i wasn’t the only one.

  • @prmonkey0123
    @prmonkey0123 ปีที่แล้ว +1

    yesterday before the video was removed, I saw a yellow Skyline, unable to tell what model

  • @celticsin4
    @celticsin4 ปีที่แล้ว +1

    Did you see that whistlindiesel destroyed the rear diffuser on the huracan he bought from you

  • @andreadepre4863
    @andreadepre4863 ปีที่แล้ว +1

    13:28 doesn’t it look like the valve has a chunk missing next to where he’s pointing

  • @PinkuStyle
    @PinkuStyle ปีที่แล้ว

    All good champ it happens. Ive had a good run with RBs. Many years also broken some. We drive them it will happen. See ya at Laguna. Ps
    You can rotate the engine with the alternator or power steering pulley.
    The compression test wws definitely wrong. Best is testers in each cylinder one shot and done and or all plugs out, fuel disconnect (cas plug) WOT test.

  • @aarongarner8452
    @aarongarner8452 ปีที่แล้ว +2

    That being one of the nismo special specs call them they might rebuild it

  • @MattMatt77
    @MattMatt77 ปีที่แล้ว +2

    Happy to see it finally Uploaded. Because yesterday was taken down.
    But because everybody knows more about cars than me and because I'm wrong why is it such a big deal if you shift into a wrong gear why would that hurt the engine?
    I would likely get a copy and paste reply from Google😂🤣💀

    • @IAmPyrofan
      @IAmPyrofan ปีที่แล้ว

      I know very little. But just from watching car channels. You shouldn't redline the engine. And when you shift down into a lower gear when you meant to go higher, the rpms are going to spike and more than likely rip past the redline. Which can cause the problems shown and explained in the video.

    • @MattMatt77
      @MattMatt77 ปีที่แล้ว

      @@IAmPyrofan Well what happens is that if you go from let's say 2gear back back in to 1gear. Let's say redline is 5k. You would be at maybe/likely 11k rpms in 1gear. That would put crazy high stress on every single part of the car Engine and transmission side.
      So over all it's very bad. This is also why I only like automatic cars. Because I have a hard time seeing what gear I'm gonna go in if it's not a gated shifter. I do know how to drive manual I also have manual bikes. But to me it's a lot easier because you don't have mistakes like this.
      But that's coming from a person like me that's on the spectrum so somebody can easily argue and say that I'm wrong because I'm not good at arguing 😑

  • @Neon041990
    @Neon041990 ปีที่แล้ว +1

    I genuinely wonder if any of these guy actually like Tommy or are just using him because there's no other alternative. Could he have been anymore condicening on that phone call. Maybe just explain what they did wrong without being a dickhead. The guy seems like a bottom feeder

    • @nungchuka
      @nungchuka ปีที่แล้ว

      absolutely, what a toss bag. He thinks his JDM, but just a biter

  • @Apexlegendzz
    @Apexlegendzz ปีที่แล้ว +1

    Suprise suprise another blown scamyeah rb 😂

  • @IxtheDuckyxI
    @IxtheDuckyxI ปีที่แล้ว +1

    You sound defeated in this video I'm sorry to hear. As a fellow GTR owner I can tell you they will always give you problems lucky you have lots of money to fix this

    • @mac_19
      @mac_19 11 หลายเดือนก่อน

      What kind of problems? Can you describe

  • @christopherharris6005
    @christopherharris6005 ปีที่แล้ว +1

    Awesome video as always TJ Hunt and Crew. It's going to be all good TJ. Like you always say keep moving forward.

  • @ricardogonzalez2861
    @ricardogonzalez2861 ปีที่แล้ว +1

    13.26 is that a piece of the valve missing?

  • @12mstokman
    @12mstokman ปีที่แล้ว +2

    13:28 isn’t that a chipped exhaust valve?

  • @easye47
    @easye47 ปีที่แล้ว +1

    The second TH-camr car Tommy scamyeah has messed up 😂

  • @calvinchau6873
    @calvinchau6873 ปีที่แล้ว +1

    RB26 problems. Thank God for the 2JZ

  • @Aldama5523
    @Aldama5523 ปีที่แล้ว +1

    Just put some rad stop leak and ship it lmao

  • @walther89
    @walther89 ปีที่แล้ว +1

    Fly Josh out.... or not but damn unlucky, dont be that excited to shift, just chill :)

  • @TH4TKIDD
    @TH4TKIDD ปีที่แล้ว +1

    Did anyone else notice the yellow R 34? 👀👀👀

  • @Supra_Mickey
    @Supra_Mickey ปีที่แล้ว +2

    Definitely would recommend the OTC compression and cylinder leakage tester

  • @loan-shark
    @loan-shark ปีที่แล้ว +1

    more money more problems !

  • @BrianCrofoot
    @BrianCrofoot ปีที่แล้ว +2

    I’ve built a couple RB’s that are still living at high horsepower. What you should really do is deck the block and head, and use a Nitto head gasket. They are basically an O-ring style gasket that work great at high horsepower. They just need a fresh/flat surface to work properly. Also, I always set the head on the dowels and then insert/finger tight the head studs. Torque up the nuts. Start the engine and let it warm up. Dump the oil and then rip the valve covers back off and retorque the head studs after a heat cycle or three. Also, not money shifting helps a lot. Something, something mechanical sympathy. Screw that, I plan on CRUSHING on my 2.8 Nitto build. Good luck bro. Love the RB content.

    • @duanebailey6253
      @duanebailey6253 ปีที่แล้ว

      The smart play would have been going to a reputable builder and use what he recommends for the build. Would have been a quarter of the price and handle way more power. N1 crank with aftermarket rods and pistons for the win. No twin turbo nonsense. Way less heat and no need for low end tq in a turbo car.

    • @BrianCrofoot
      @BrianCrofoot ปีที่แล้ว

      @@duanebailey6253 I agree. I’ve used the same engine builder for 2-3 RB builds, with great luck. And all of my builds, including my current Nitto 2.8 stroker have been single turbo. My new build is also going shimless bucket, which I’ve never done before, but I’m hoping I will be able to rev this bad boy to 9k rpm or higher if it’s still making power up there! Just trying to help TJ because not many people build RB’s over here yet, and they require almost no margin for error. His HKS stroker would have probably been fine if he didn’t money shift, living at ~600whp, but since it’s all apart, I would recommend doing what I said. Get it to a machine shop, get it all checked and decked, and re-torque the head again after a few heat cycles before turning up the power.

    • @Crazy_CAT16
      @Crazy_CAT16 ปีที่แล้ว

      It's true that it's difficult if you don't know what to ask or ask for advice on the RB engine, this is the same thing that Adam experienced when he first had an R32 sedan and he met the GDR god Andrew Hawkins
      @@BrianCrofoot

  • @Milo04006
    @Milo04006 ปีที่แล้ว +1

    TJ Is that a Yellow R34 I see!??👀👀👀

  • @JaimeMedina11
    @JaimeMedina11 ปีที่แล้ว +1

    Please take care of this car it’s a dream for most of us :)

  • @thejasonstackhouse
    @thejasonstackhouse ปีที่แล้ว +1

    Surely I'm not the only one who saw that the intake valve below Tommies finger at 13:42 is broken and has a clear chip in it.

    • @thejasonstackhouse
      @thejasonstackhouse ปีที่แล้ว +1

      1000% broken valve on intake cylinder 4. I just zoomed the video in to make sure it wasn't grease or something dark sitting on the valve, it's not I can clearly see the metal is sheared

  • @davidmasseria8687
    @davidmasseria8687 ปีที่แล้ว +1

    13:27…is one of the valves cracked? Or am I seeing dirt or grime on it making it look that way?

  • @Binceymusic
    @Binceymusic ปีที่แล้ว +2

    15:05 yellow skyline with pink rims? o.O

  • @Rui_Goncalves78
    @Rui_Goncalves78 ปีที่แล้ว +1

    Uhhhh a yellow r34 at the end 😍

  • @ultimatespartan6244
    @ultimatespartan6244 ปีที่แล้ว +1

    when you striped the motor the first time was there not already a blow head gasket - and when you guys assemble it did the measure the block and inspected in-between the a straight edge and a feeler gauge or did you just assembled it before assembling this engine please measure and do a die test on the block as well by dyeing the block and taking a marble counter top that is straight and run it back and forth to take the die of and if all the die comes of its right but if there is still die on between the cylinders then you now you have a low spot as well check on the head of any low/high spots you can check by just you're eyes

  • @jongib6096
    @jongib6096 ปีที่แล้ว +1

    Rookie move man. Not cool 😅👎🏼

  • @Minebiowerz
    @Minebiowerz ปีที่แล้ว +1

    spaced metal head gaskets are the way to go, Turbo L series motors only last with them because the extra space allows a more forgiving combustion gap, and the metal has a lower chance of blowing out.

  • @patrickjohansson3076
    @patrickjohansson3076 ปีที่แล้ว +1

    Yea 14:28 we see the yellow body kit

  • @ninomatancillas4278
    @ninomatancillas4278 ปีที่แล้ว +1

    Was that a yellow 32 at the end 🤫

  • @00MsaM00
    @00MsaM00 ปีที่แล้ว +1

    Get a Fire ring head gasket.

  • @mikesone64garage
    @mikesone64garage ปีที่แล้ว +1

    14:29 another R34 or R33 GTR? 🤔

  • @ultimatespartan6244
    @ultimatespartan6244 ปีที่แล้ว +1

    as well as on you're tune file on first gear what is the flow rate se for fuel it might have gone into first gear and requested more fuel causing detonation with over fuel pressurizing and then blow the head gasket

  • @GermanEliteTuning
    @GermanEliteTuning ปีที่แล้ว +1

    Hug bummer but the issue could have been way worse. The Bloopers were great. You should bring them back in every vid 🤘🏻🤘🏻

  • @evanmlevy
    @evanmlevy ปีที่แล้ว +1

    Crazy I thought you posted this yesterday but couldn’t find it!

  • @gorto90
    @gorto90 ปีที่แล้ว +1

    Honestly gotta say, very sad this happened but this is one of the MOST interesting video you ever put out, digging deep into a rb26 is really fascinating, learned alot

  • @shaunknysh3330
    @shaunknysh3330 11 หลายเดือนก่อน

    Stop scratching your head 😾 😾 and start scratching your balls 🏈 🏈 bro😮..... could be a sack issue 😕😅🐔🐔🍗🍗if thats not it id suggest double head scratching fallowed by a ball tap or 2 and repeat 🐔🍗🐔🍗 if the ball tap dont fix it ....... wait a second😮😮....... why the hell you even listening to me im no macanic 😅😂😹 😂 TJ I really hope this helps. I mean these are the only suggestions I can offer 🫴🫴🫴🫴🫴🫴🫴😮 that's 2 taps 1scratch fallowed by 2 of the same ...happy tapping 😂😂😂

  • @mrsquirrel8079
    @mrsquirrel8079 ปีที่แล้ว

    I bet a 2JZ wouldn't have this problem after a mistake...jus sayin.... what about the coil pack?
    If compression is good then why check the mechanical side...???

  • @drewsoxfan04
    @drewsoxfan04 ปีที่แล้ว

    At least it seems better-ish than my situation! I just blew the motor on my 18’ wrx, no warranty, $10k quote for a new one when I still owe $12k on the car…also paycheck to paycheck unfortunately. Can you say fu*ked??