power divider rebuild mystery dsp41

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  • เผยแพร่เมื่อ 30 ม.ค. 2025

ความคิดเห็น • 167

  • @DoggyDogYT
    @DoggyDogYT 11 หลายเดือนก่อน +17

    This guy knows his stuff! Man we need more men like him! Taking pride in his craft! God bless you brother!

    • @davidpawson7393
      @davidpawson7393 11 หลายเดือนก่อน +3

      I haven't, currently don't and never will own a commercial truck but I'm here because he handles business himself and builds what he wants. I completely agree with the world needing more like him.

    • @lionsdejudah
      @lionsdejudah 7 หลายเดือนก่อน

      He just said himself at 11:57 that he didn’t know much about rebuilding the power divider.

    • @lionsdejudah
      @lionsdejudah 7 หลายเดือนก่อน

      Those gears didn’t need to be replaced as stated by the repair shop he took them to.

  • @mitchless1589
    @mitchless1589 11 หลายเดือนก่อน +11

    check airflow/pressure to the actuator. sometimes I put a few drops of air tool oil in it too

  • @signalcar
    @signalcar 11 หลายเดือนก่อน +13

    The good side of not having parts with serious damage shows how well the truck is cared for and well driven, certainly that fork and those chewed splines did the bad thing, in any case it's good to know that all the splines on the axles are fine and the set is revised. Keep up the good work, greetings from Brazil!

    • @carlthor91
      @carlthor91 11 หลายเดือนก่อน +1

      As you mentioned, plus a possibly weak actuator, and the dogs can't engage properly, so the jump.

  • @peteengard9966
    @peteengard9966 8 หลายเดือนก่อน +6

    Had one doing the same thing. Turned out the hose to the actuator was collapsed inside not giving it the volume of air it needs to overcome the return spring and keep it engaged under load. I went through the same thing you did but only changed out the fork. Then tied in an air gauge under the actuator inlet and only got 30 psi but climbed up slowly to 120 after about ten seconds. That was the moment I realized the inside of the hose was falling apart. There was little bits of rubber jammed in the elbow going to the actuator.

  • @JamesPretty
    @JamesPretty 11 หลายเดือนก่อน +9

    Frustrating to spend all day and in the end hope it’s fixed. Great job as always

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +4

      Sure would have liked to have found a smoking gun but so far it seems to be fixed 🤷

  • @etcllc3519
    @etcllc3519 11 หลายเดือนก่อน +1

    We love your videos and how you share your knowledge with the public. Sorry to say, we are closing our business and getting out of the industry. 29 years is enough! We’ve got a 94’ KW 900 for sale ($40k) with a CAT 3406B that has 67k on a fresh inframe with all CAT parts and done by a CAT dealer. Too many new parts to list but have receipts for everything for the past five years! Should you know anyone interested up there in farm country, please let us know. Keep up the good work and God bless.

  • @raymondbradley6788
    @raymondbradley6788 11 หลายเดือนก่อน +8

    Ezra, that is frustrating to not find something catastrophically wrong. Hopefully you nailed it. Sounds like that might’ve been what we were going on but only will know under a load. Awesome video brother. Thanks.👍👍👍

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +3

      Would have been nice to find a smoking gun

  • @kidsteach938
    @kidsteach938 11 หลายเดือนก่อน +3

    Nice episode, Ezra. I was beginning to think the same way...that the divider was not fully engaged. That shift fork just might explain things. Good luck and look forward to seeing how it all works out!

  • @bigmackstruckstop9213
    @bigmackstruckstop9213 11 หลายเดือนก่อน +1

    Good to see you Ezra, thank you for the education of your 359 peterbilt, there's stuff I didn't know about,I know I can learn from you and your show, so I'll catch ya on the next one 😊

  • @lox_501
    @lox_501 11 หลายเดือนก่อน +2

    Great job the bud. It's nice to see what a differential looks like on the inside. Massive gears!

  • @marysoldeeley2218
    @marysoldeeley2218 10 หลายเดือนก่อน

    Good thing you remembered to drain the oil before it poured out onto you! That's always a bonus! Well, this sounds like a Big Red Mystery! This was a great learning opportunity! Now if there is any other issues with power dividers. You will know what you are getting into, what to check and what to expect! Thanks for showing us all this! I was curious what all that looked like in there all put together!

  • @ronthompson3525
    @ronthompson3525 11 หลายเดือนก่อน +4

    Well sometimes just throwing parts works. But it’s frustrating when you can’t actually find something wrong. Hope the issue is resolved. Take care ✌️

  • @billtodd6509
    @billtodd6509 11 หลายเดือนก่อน +6

    EZ, I had one IH do the same type thing with us and here the leveling valve would sometimes let enough air out of the bags to change the angle on the driveline enough to give you that seat of the pants feeling of the truck seeming to squirm when you were on soft ground, Bill

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +2

      This was a obvious slip and then bang back in. Very different than a u joints bind or vibration

    • @billtodd6509
      @billtodd6509 11 หลายเดือนก่อน +1

      Im sure that you will get it sorted out. Let us know if problem goes away.@@Ezrider359

    • @stephenrichardson6105
      @stephenrichardson6105 11 หลายเดือนก่อน

      Soon as you took it apart and found nothing obvious I was wondering if it was the actuator/folk not holding the gear and jumping
      Banging in and out

  • @mikemaccracken3112
    @mikemaccracken3112 11 หลายเดือนก่อน +1

    Thanks for the video Ezra. I know exactly how you feel when I have to use my best educated guess when I didn’t find the clear failure.

  • @SumterWrecker
    @SumterWrecker 11 หลายเดือนก่อน +1

    Mr Ezra Thanks for sharing and stay safe

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน

      thanks for watching hal

  • @koshtie
    @koshtie 11 หลายเดือนก่อน +1

    Hi Ezra that sure was a strange one ? nothing stood out, Fingers crossed she's all good,
    ATB Wayne UK......

  • @ponway
    @ponway 11 หลายเดือนก่อน +4

    Had a DS 404 doing the same same thing, I kind of wondered if it wasn’t fully locking up. But before I tore into it, I ended up doing a cut off swap like you did, and it’s laying out back yet to be investigated!
    Great work!

  • @shanedrives8934
    @shanedrives8934 3 หลายเดือนก่อน

    This is a great video, thanks for doing this. I'm getting ready to tear into my DS404, basically the same setup. Pretty sure my spider gear just went out today.

  • @Mike-xt2ot
    @Mike-xt2ot 11 หลายเดือนก่อน

    I admire your knowledge and work ethic. Top shelf. Nice rig !

  • @RobertGilmour-ju7mv
    @RobertGilmour-ju7mv หลายเดือนก่อน

    Yep,mate I have been a truck mechanic for 40 odd years I know how you feel there is nothing worse than not finding anything drastically obvious and most of it looks ok its abit like the old saying the tooth ache goes away as you walk in the door. Best of luck take care.

  • @HODGEPODGEDODGEGARAGE
    @HODGEPODGEDODGEGARAGE 11 หลายเดือนก่อน

    I'm glad it seems to be fixed now Ezra, that looked like a *BEAR* to mess with. Hats off to you for doing the work yourself my friend! 🔧🔩

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      Thanks for watching Zane 👍

  • @mgtowquietearp506
    @mgtowquietearp506 11 หลายเดือนก่อน +9

    I found on my 94 379, the air actuator had an air leak and wasn't engaging the shift fork completely!

    • @abc-jd9se
      @abc-jd9se 11 หลายเดือนก่อน +3

      That’s my thought too. Binding actuator, leaking actuator, restricted air line, etc

    • @budatkins5917
      @budatkins5917 11 หลายเดือนก่อน

      Thats where I was going too@@abc-jd9se

  • @hankhill3263
    @hankhill3263 11 หลายเดือนก่อน +1

    You're fu**in awesome bro, thanks so much for the video, I know its probably a pain in the ass making these videos while you're doing important work like this, I just wanna say I really appreciate your videos and your effort Ezra, the hardest working and smartest man on TH-cam!!! Just puttin it out there - we know you're busy out on the road every week but I'd love to see what you do thru the week too, if ya get the chance can ya get some footage of your day to day work activities? Thanks again ol buddy - can't wait for your next videos!!! Be careful out there ol buddy!!!

  • @DaveDettmann-v3m
    @DaveDettmann-v3m 11 หลายเดือนก่อน

    a bore scope could probably get in to see the differential spider gears. Harbor Freight ones are not too bad a picture. Good to see another video! Cheers

  • @robertquast9684
    @robertquast9684 11 หลายเดือนก่อน

    Our 377 runs ds 402 rears. We had a bunch of power divider problems after changing the original. Finally went to a different reman place. Never figured out what they were doing wrong but 100k pounds self destructs them pretty quickly and throughly. Hopefully it’s fixed so you aren’t down in season

  • @randystrunk9774
    @randystrunk9774 11 หลายเดือนก่อน

    I'm going through the same thing. Same rearends. We replaced the spider gears & the pieces they run in & so far we havent had any issues. The spider gears were loose on the pins they go through.

  • @nightrider6769
    @nightrider6769 11 หลายเดือนก่อน

    Hi EZ. Seen the inside of a differential is a on a truck is a first for me the shops I've worked at over the years most of the trucks were fairly new equipment and they had warranties so if you had an issue they'd go to the dealer so we never dealt with tearing them down the only thing we did is change oil in the diffs and when you pulled your plugs out what I saw on the end of your magnet there look perfectly normal I've seen that all the time when I was changing diff oil so I it didn't grenade big or anything I agree with you I didn't see anything that would alarm me by any means but I wasn't there in person feeling it I was just using my eyes but everything looked really good and that power divider I'm very surprised at Hull straightforward that was I mean that did not look difficult to do I bet the gears weren't cheap but you know to put the new stuff in look pretty simple something I'd never done but hopefully you got the situation fixed I guess we won't know for 5 months from now maybe you can do a video on updating us how it's doing if it's still doing it or it's not doing it that'd be wonderful but thanks for bringing us along on this tear down and put back together I enjoyed it immensely.

  • @michelgodin5563
    @michelgodin5563 11 หลายเดือนก่อน +3

    you make my sunday, glad for video

  • @CMDSR
    @CMDSR 10 หลายเดือนก่อน

    I think a good gear jammer started noticing there was a problem and corrected it before major damage occurred. Good thing you didn’t find any major damage there driver. Bad thing no major damage makes it harder to find a cause. Hope that fixes the problems in soft ground.

  • @jay600katana
    @jay600katana 11 หลายเดือนก่อน

    Another good video, good to see ol'red. Throwing parts at shit until its fixed sucks, I had a trailer that I did that with. Hope everything works out, keep the wheels spinnin' and the beavers grinn'in bud.

  • @richardherbert6665
    @richardherbert6665 11 หลายเดือนก่อน

    Thanks for the update! Hope everything works out!!

  • @ricbrowne3249
    @ricbrowne3249 11 หลายเดือนก่อน

    .Hi Ezra I had a similar problem with a highway truck that was about 14 yrs old it had done well over 1. 5 Million Kilometers I could feel the transmission jumping what seemed to me gears jumping over them selves , I took the truck to the service Dept. because the back diff oil was a bit brassy looking they changed the rear diff , long story short it turned out to be the gear box , we ended up re-racing & replacing some of the gears in the box . "18 speed Road Ranger " solved the problem , just a thought mate . cheers "RB" Albury Australia

  • @tater_relocater
    @tater_relocater 11 หลายเดือนก่อน +1

    My thought was the actuator wasn’t working properly and overcoming the spring pressure on the fork.

  • @jims6323
    @jims6323 11 หลายเดือนก่อน

    How about the piston that engages the clutch blowing by?

  • @re9947
    @re9947 11 หลายเดือนก่อน +4

    Keep us posted Chivo.

  • @trevorthompson2501
    @trevorthompson2501 11 หลายเดือนก่อน

    Replace o-ring in the front cover you pulled off. It’s what slides the shift fork back and forth. They get old and worn and can have a hard time engaging the power divider or not engage it at all.

  • @alecc3094
    @alecc3094 11 หลายเดือนก่อน

    In UK that power divider is called an inter axle diff lock and for many tears now double drive bogies like this one would also have a cross lock on each axle to make both wheels drive together. Worked really well in a staight line but a typical 3 axle rigid would not respond to the helm on slippery surfaces so you needed to disengage asap.

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน

      potato potato, both terms are used here no cross locks on these rear ends. i may put at least one cross lock in a some point.

  • @matthewhansen5008
    @matthewhansen5008 11 หลายเดือนก่อน

    I had some engagement issues on a dsp40 rear end. You could hear air leaking into the rear end housing with the truck turned off and divider locked in.
    Replaced O ring on engagement piston. Fixed my troubles.
    Just a thought that could be a slight leak and it not be holding the piston down tight and allowing the teeth to skip under heavy load.

  • @donrotenberry6571
    @donrotenberry6571 11 หลายเดือนก่อน

    Hello Ezra. been a while. Hope this fixed your problem. Everything else looked OK. Be Safe & Stay Warm.

  • @wotnoturbo
    @wotnoturbo 11 หลายเดือนก่อน +1

    Check the air pressure at the actuator when its engaged, the only thing holding the teeth in mesh is whatever the air pressure is set too, if this is too low that may cause the teeth to cam out under load.

    • @youtubeisawesome2487
      @youtubeisawesome2487 11 หลายเดือนก่อน

      some trucks set it up to run only in low side of the transmission and you only get the 65 psi from the regulator, very dumb but keeps idiots from burning it up from forgetting to turn it off .

  • @nightsailor1
    @nightsailor1 11 หลายเดือนก่อน

    Is the clutch moving sharply and holding location? Is it worn? Is the supply correct and the delector switch like new? does it disengage positively?

  • @RMTTR640
    @RMTTR640 11 หลายเดือนก่อน

    What was the end play on the input shaft when it was all reassembled?

  • @Xkekeskfndsmw
    @Xkekeskfndsmw 9 หลายเดือนก่อน

    Any updates? Have you found a situation to test the issue yet? Spring break-up might put it to the test?

  • @Mark-g3k8b
    @Mark-g3k8b 11 หลายเดือนก่อน

    Thanks for the info you give you are great at the work you do good job 👍

  • @slooo9
    @slooo9 11 หลายเดือนก่อน +1

    Dont forget to let us know if its corrected. Be safe out there....

  • @garykirk1968
    @garykirk1968 11 หลายเดือนก่อน +3

    Does the truck have locking differentials? Could be one of those, the power divider just connects the front and rear tandems, if one locker or the other is slipping Could cause an issue similar to what you're describing.
    Edit to add; You could also put a pressure gauge on the air input back there, make sure it is getting full system pressure. Low air pressure for whate er reason can cause it not to fully engage.

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      No cross locks pressure was checked previously

    • @mikesautotruckrepairinc.cr5621
      @mikesautotruckrepairinc.cr5621 11 หลายเดือนก่อน

      @@Ezrider359 Usually something like that will not be pressure related due to the back cut on the dog clutch notches.Not sure if you used genuine parts but possibly a revision on the notches eg revisions on Mack syncro hub tooth design.Good luck.

  • @largesleepermadness6648
    @largesleepermadness6648 11 หลายเดือนก่อน

    As mentioned in the thread, the air actuator for the diff lock was an issue on my 2006 kw.

  • @goldprogoldpro7809
    @goldprogoldpro7809 11 หลายเดือนก่อน

    could it be low/leaking/blocked air pressure to the shift fork?

  • @simonharris1804
    @simonharris1804 11 หลายเดือนก่อน

    What transmission do you have
    Is it a fifteen speed with deep reduction
    When it was in deep reduction it would kick out by itself with a almighty bang back into gear
    Could be air related not enough pressure or wear on selector synchro
    Might be worth checking
    Only did it loaded

  • @Go4BrokeOffroad
    @Go4BrokeOffroad 11 หลายเดือนก่อน

    Always very helpful videos. 🤘

  • @tossedsalad5532
    @tossedsalad5532 11 หลายเดือนก่อน +3

    There is 1 thing for certain you get a TAX break on all the cash spent on parts.
    All Joking aside U-Joint issue even if they are New some lock or Hitch causing that type of issue.
    We had 1 U-Joint mystify us while we rebuilt A tons on rear end components.
    End result was U-Joint and a out of alignment Differential causing the problem. The diff was out of Alignment and cause a U-Joint to intermittently bind

    • @edtoebes
      @edtoebes 11 หลายเดือนก่อน

      I was thinking the same thing. If a joint was sticking and under pressure it was skipping, it might cause what he is sensing

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      Not the issue here but appreciate the input

    • @hankhill3263
      @hankhill3263 11 หลายเดือนก่อน

      ​@Ezrider359 I was not a driveline mechanic at all, I was lucky enough to have some mechanics near me that specializes in everything in the driveline, they always kept me pretty well straightened out, I always had enough sense to know when there was a problem so I just took it to them and they always knew the problem right away - Midwest Rebuilds in Fort Recovery Ohio, great bunch of guys there if anyone ever needs any help from that area

    • @ryancarter7167
      @ryancarter7167 11 หลายเดือนก่อน

      I had one skip like that under load and the fork was bent and worn. Mine had wear in the compensator that made excessive clearance but seems like the slider needs to e gauge all the way for a solid lock.

  • @matthoward923
    @matthoward923 11 หลายเดือนก่อน

    Just got done replacing the power divider on my truck two weeks ago. Lost the front bearing at the yoke. My back hurts for you.

  • @mattheusbeukes6809
    @mattheusbeukes6809 11 หลายเดือนก่อน +1

    Hi EZ I had that problem one time and it was the valve that didn't send enough air through and I also stripped like u and saw nothing

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      Valve and supply pressure was checked long before tearing into it

  • @tommyhall2768
    @tommyhall2768 11 หลายเดือนก่อน +2

    Hellow buddy an Ole red good luck

  • @randystrunk9774
    @randystrunk9774 11 หลายเดือนก่อน +1

    If you want to test it, remove the rear driveshaft & drive it on the front rear. Mine showed itself real fast.

  • @ericcorse
    @ericcorse 11 หลายเดือนก่อน

    Finger crossed you fixed it.

  • @matthew6202
    @matthew6202 7 วันที่ผ่านมา

    Great video 👍

  • @keepontruckinoutlawlife1248
    @keepontruckinoutlawlife1248 11 หลายเดือนก่อน

    Ezra you do great work thanks for sharing as always appreciate ya driv,ah.

  • @stevencampanella
    @stevencampanella 5 หลายเดือนก่อน

    I am having the exact same issue. Did this fix it?

  • @sixtoes2313
    @sixtoes2313 11 หลายเดือนก่อน

    Good luck EZ. Hope ya got it.

  • @cameronnerdin4910
    @cameronnerdin4910 11 หลายเดือนก่อน

    AHHH THAT SINKING FEELING WHEN YOU SPENT A BUNCH OF TIME AND MONEY, and your not sure if that was the problem. Been there done that. I hope the problem was the slow or catching engagement. Seams to be a possibility. I know, when I engage my lock, I never so it while moving. I also stop to disengage them. Most people say you do not have to, but so far no problems with mine. I feel for you.

  • @derrickhillier1173
    @derrickhillier1173 11 หลายเดือนก่อน +1

    What's the issue Your having Ezrider?

  • @buddyreed2623
    @buddyreed2623 11 หลายเดือนก่อน

    If it's two months before the ground thaws, be sure to let us know and perhaps try to get to the same soft spot and weight on the fifth wheel to see if it does the same thing. Have good days!

  • @gasperajdnik8004
    @gasperajdnik8004 11 หลายเดือนก่อน +1

    Good work 👍

  • @Jerseytrucker911
    @Jerseytrucker911 11 หลายเดือนก่อน +2

    👏👏👏🤜🤛.. great job, thanks for sharing!

  • @tomgriffith1952
    @tomgriffith1952 11 หลายเดือนก่อน +1

    Nice work!

  • @russellgier5489
    @russellgier5489 11 หลายเดือนก่อน

    I had one do the same thing and it was a combination of the thrust washer, shifter collar and arm

  • @rce8540
    @rce8540 11 หลายเดือนก่อน

    Great show easy Ryder.

  • @mudpuppy2158
    @mudpuppy2158 11 หลายเดือนก่อน

    mine did same thing and it was side bearing that holds ring gear

  • @joshrappl4878
    @joshrappl4878 7 หลายเดือนก่อน

    From what you are describing it sounds like 2 teeth are broken off of the ring gear hard to inspect it good with out pulling diff. Pinion makes contact with 2 teeth while spinning. Generally one tooth could be broken for years and never know. Once the second consecutive tooth breaks you might get gear jump like you are talking. Then shock loading issues. Was almost sure it was a ring gear when I started watching. Was off my rocker when you didn't pull the diff to check ring gear. I'm a belly dumper so soft ground and broken diffs are just part of the game. Most of the time for us it is a broken ring gear or spider gear.

  • @boevatt9152
    @boevatt9152 11 หลายเดือนก่อน

    Wouldn't it be the backside to drop the back driveway

  • @saddletramp1979
    @saddletramp1979 11 หลายเดือนก่อน

    Makes me wonder about the part that puts it in gear, maybe its not working right,

  • @mjkrigging6374
    @mjkrigging6374 11 หลายเดือนก่อน

    Was it an air problem

  • @PowerOfValmet
    @PowerOfValmet 11 หลายเดือนก่อน

    Now i dont drive a american truck but in some cases on scanias the shift fork can bend and then it behaves like yourse, or the the thing that moves the fork doesnt have the power to hold the shift fork in place so it skips. But hope it works for you buddy 😊

  • @stevenpoff6273
    @stevenpoff6273 11 หลายเดือนก่อน

    Well hopefully that fixed the issue that you were having😊😊

  • @DON-T909
    @DON-T909 11 หลายเดือนก่อน

    Hi Ezra
    Another great learning video Thanks, What was your actuator like ? maybe that was jamming ? just a thought
    Hopefully you have it fixed now, Take Care

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      nothing apparently wrong. its just a cap a piston and a couple o rings it was cleaned new seals and checked for function

  • @elljay4587
    @elljay4587 11 หลายเดือนก่อน

    Need to look into the transmission

  • @joestreiff9401
    @joestreiff9401 11 หลายเดือนก่อน

    what would be the cost of a used power divider, as compared to the new gears?

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      I don't know but why put labor into used parts that probably aren't any better than what came out

    • @joestreiff9401
      @joestreiff9401 11 หลายเดือนก่อน

      @@Ezrider359 well technically you started out with used parts the moment you chose to weld on the ass section of the truck.
      I've seen "new" parts fail more often that we care to realize.

  • @hammers1518
    @hammers1518 10 หลายเดือนก่อน

    Hope all is good Ez

  • @CA-fn1wg
    @CA-fn1wg 11 หลายเดือนก่อน

    Pull the output yoke and input on the rear drive axle see if yokes are worn when they load up the splines and can jump. Then normally they die then. yokes are softer metal then the shafts. No poping when 1st to reverse fast, not sounding like a carrier bearing, that will blow a axle shafts. power divider have full truck air pressure i believe it should just not holding the shift fork tight? Or letting the collar loosen up, or not tight enough 15 plus years of big truck shop time thinking.

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน

      every single splined shaft was checked in the entire driveline there was a lot more checking stuff than just what was shown in the video. air pressure was checked long before tearing into the power divider. good suggestions though.

  • @victorchavez1760
    @victorchavez1760 11 หลายเดือนก่อน

    How much were the parts you replaced?

  • @randyraterman3869
    @randyraterman3869 11 หลายเดือนก่อน

    Hope it’s fixed Ezra, but if it’s not check the actuator and the air valve the feeding the actuator. It would be a real pisser if it was just a pinched air line somewhere after all that work.

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      Was checked long before tearing into the power divider

  • @edwarddavis507
    @edwarddavis507 10 หลายเดือนก่อน

    EZ did you sell your Mack

  • @johndemeen5575
    @johndemeen5575 11 หลายเดือนก่อน

    Some kind of metric. Million thanks for entertaining me. St.Paul,Minnesota.

  • @katmandu8208
    @katmandu8208 11 หลายเดือนก่อน +1

    👍🏻🍻

  • @69hayes48
    @69hayes48 11 หลายเดือนก่อน

    transmission ?

  • @vincentstanley68
    @vincentstanley68 11 หลายเดือนก่อน

    Are you somewhere in the midwest?

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      north Dakota

    • @vincentstanley68
      @vincentstanley68 11 หลายเดือนก่อน

      @@Ezrider359 i like how you fix your truck! Good luck with the power divider! You inspire me to keep on going when im not confident cuz ive never done it before. Keep the videos coming please

  • @JorisV1983
    @JorisV1983 11 หลายเดือนก่อน

    Im no expert on these things. However i am a mechanic and what i see is that the ring that engages the power divider is way to lose on the splines it is on.
    Edit: i just saw you put the old rong back on the new shaft arount 21:36. I woud have put a new one on. Seems way to loose.

  • @eddieweigel9490
    @eddieweigel9490 10 หลายเดือนก่อน

    Great job

  • @LightningFabrication
    @LightningFabrication 11 หลายเดือนก่อน

    Hey Ezra, it's got to be frustrating that there wasn't a definite problem that presented it's self when you took the power divider off. I know you wanted to check the spider and axle gears in the differential but that would have meant pulling the 3rd members. However on the front differential you could see the housing and the ends of the spider gear cross. If you wanted you could have installed one axle and spun the the pinion. The axle would have held the axle gear steady while the spiders and other axle gear turned. Doing this would have let you feel if there was any binding. In my opinion if any of the spider gears were broken, you wouldn't have any movement either forward or reverse if there were damage to the spiders in the rear differential. if there were damage to the spiders in the front differential you wouldn't have forward or reverse with the power divider unlocked but if locked you would have forward and reverse through the rear differential.
    I think you might have found the problem. With the wear on the fork and the splines on the shaft being a little buggered up, the shift sleeve might not have been fully engaging. When all the torque was applied, there might have been enough force on the fork to overcome the tension on the spring allowing the sleeve to disengaging the power divider. When the power divider isn't engaged power is routed to the wheels on both axles with the least traction. There is still torque on both axles so I'm thinking that there might not be as much damage to the sliding sleeve when it popped . Just a theory which might explain why there wasn't catastrophic failure. it will be interesting to hear if the repairs fixed the problem.

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      i did check the spiders on both rear ends by spinning them with one axle and feeling for any excessive lash or crunchyness or anything like that. i didn't really feel that that would be a issue anyways as on level ground with even traction you can apply enough torque to just about pick the front wheel off the ground and nothing will skip or jump, it was only when applying a load on the powerdivider itself. this video was recorded about a month ago and its been working fine but i probably really wont know for sure if its fixed till we get into road construction season

    • @LightningFabrication
      @LightningFabrication 11 หลายเดือนก่อน

      @@Ezrider359 Okay glad to hear it's been working well. I hope it will continue to work later during construction season.

  • @anastasiszaroliagis5066
    @anastasiszaroliagis5066 9 หลายเดือนก่อน

    Remember always, if tyres of 1st and 2nd axle have uneven wear the system didnot work properly...do not waste your time...😊😊

  • @LouisRoman-p7y
    @LouisRoman-p7y 11 หลายเดือนก่อน

    Thanks for sharingl

  • @markchodroff250
    @markchodroff250 หลายเดือนก่อน

    I would replace the shift fork and the Measure the fork throw with the air Solenoid

  • @isaacsims6203
    @isaacsims6203 10 หลายเดือนก่อน +1

    🙂

  • @rdavila26
    @rdavila26 11 หลายเดือนก่อน

    I had something similar happened to me , turn out it was a worn out yoke on the drive line

  • @josh33025
    @josh33025 11 หลายเดือนก่อน

    Good ole parts cannon. Hopefully it does something positive.

    • @Ezrider359
      @Ezrider359  11 หลายเดือนก่อน +1

      Nothing like throwing over $800 in parts at something and hoping it's fixed. Sure would have liked to have found a smoking gun but it has been over a month sense the video was recorded and haven't had a issue with it yet. So I dunno

  • @Daves_adventures4315
    @Daves_adventures4315 11 หลายเดือนก่อน

    Wahoo Ezra video!!

  • @garygeer7646
    @garygeer7646 11 หลายเดือนก่อน +1

    😎👌

  • @snakebite2841
    @snakebite2841 11 หลายเดือนก่อน

    👍👍

  • @wadelevan1787
    @wadelevan1787 11 หลายเดือนก่อน

    I guess if enough components have a small amount of wear, the cumulative effect could be equivalent of one component with heavy wear. “Within spec” is not the same as optimal.