Blown Head Gasket Denial on this 1993 Ford Mustang - The Curse of the Black Foxbody Continues...

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  • เผยแพร่เมื่อ 25 พ.ย. 2024

ความคิดเห็น • 40

  • @JamesMason392w
    @JamesMason392w 7 หลายเดือนก่อน +7

    I use two three inch sections of all thread that I screw into opposite corners of the heads. This helps as a guide when you are placing the lower intake into position. It drops right in place.

    • @speedeetrim4028
      @speedeetrim4028 7 หลายเดือนก่อน +1

      ya I do the same...works !

  • @ogsuperflygarage
    @ogsuperflygarage 6 หลายเดือนก่อน +1

    No truer words Chris, “Troubleshooting takes time!” I appreciate your integrity and dedication to doing a great job and honestly helping your friends!

  • @ryanhuset2223
    @ryanhuset2223 7 หลายเดือนก่อน +2

    A couple longer bolts with the heads cut off make excellent dowel pins. Intake goes on straight every time

  • @Reztek302
    @Reztek302 7 หลายเดือนก่อน +1

    I use high tack gasket adhesive. Works well and sets up fast.

  • @speedeetrim4028
    @speedeetrim4028 7 หลายเดือนก่อน +1

    hey Chris I always glue my intake to head gaskets in place...then drop the intake in place using studs into the heads on the corners...threaded rod cut to length works

    • @TheInfamousProject
      @TheInfamousProject  7 หลายเดือนก่อน

      Problem is the gasket still would have dipped most likely due to the elongated holes in the gasket!

  • @chriswise1232
    @chriswise1232 7 หลายเดือนก่อน +1

    In older engine blocks, there tends to be a recession on the deck where the coolant flows through. It might just be .002 or something on this motor, but it gets worse over time until it gets decked.

    • @ollelinderholm1745
      @ollelinderholm1745 7 หลายเดือนก่อน +1

      my old ´88 5.0 302 block had an ever so slight "bump" in one end after an overheat, nothing helped the overheat issue but a potential decking of the block, but I went with a new block instead. so, What Im saying is, unfortunately new gaskets, milled heads,=no avail...nothing was enough to fix the leak bettween head and block in the one bad section...

  • @ianrs6310
    @ianrs6310 7 หลายเดือนก่อน +1

    When I did the head gaskets on my notch I threaded in old intake bolts with the heads cut off to keep the gaskets in place while I lowered the intake on. Kept everything lined up.

    • @TheInfamousProject
      @TheInfamousProject  7 หลายเดือนก่อน

      Thing was the bolt holes are slotted and still allowed the gasket to slip down!

    • @ianrs6310
      @ianrs6310 7 หลายเดือนก่อน

      @@TheInfamousProject wow. Not fun.

  • @MrMl1986
    @MrMl1986 7 หลายเดือนก่อน +1

    Wow who would have thought. Good job finding it with the camera

  • @bendirusso3149
    @bendirusso3149 7 หลายเดือนก่อน +1

    Great video. It happens to the best of us!!

  • @sammyvices2547
    @sammyvices2547 7 หลายเดือนก่อน +4

    Once you do head gaskets on your own car and learn how to adjust valve lash a couple times. Theres nothing left to intimidate you about tearing apart your own motor, it’s an awesome learning experience

    • @TheInfamousProject
      @TheInfamousProject  7 หลายเดือนก่อน +1

      Ya but it doesn't make it anymore fun... I think the only part I enjoy is Valve Lash because I do it the lazy way and it works every time lol.

    • @adammarshall4576
      @adammarshall4576 7 หลายเดือนก่อน

      Haha these ones make me laugh 😂😂. ✌🏻✌🏻

    • @TheInfamousProject
      @TheInfamousProject  7 หลายเดือนก่อน

      @@adammarshall4576 lol gets me every time bro

  • @ldh4650
    @ldh4650 7 หลายเดือนก่อน

    If it helps, I used 4 old intake bolts, cut the heads off and used them as guide pins so the lower intake installs in its exact position.

  • @jk1203
    @jk1203 7 หลายเดือนก่อน

    Great vid always enjoy your attention to detail

  • @Boxerfox714
    @Boxerfox714 7 หลายเดือนก่อน

    Bro I had a similar issue with my car overheating and sending my head to the machine shop while removing my lower intake manifold it ended up being married to my heads due to coolant passage, so i ended up upgrading my lower upper intake manifold swapping everything over huge headache on thing i found which was kinda cool it had the original head gasket from assembling line

  • @jamesrene9378
    @jamesrene9378 7 หลายเดือนก่อน +1

    Does a stock cam make a difference in a compression test? I have a fresh stock 302 and I’m getting 95psi on all cylinders. Just curious if a aftermarket cam gives you higher compression on the test

    • @TheInfamousProject
      @TheInfamousProject  7 หลายเดือนก่อน

      It would change things for sure however 95 is low but with that said if you're consistent across all cylinders that is good. Try again but make sure all your plugs are out and keep your throttle body wide open...

  • @joey4872
    @joey4872 7 หลายเดือนก่อน +1

    The Black Fox curse is true😂😂😂 I own a Black Fox😅😅😅

  • @speedeetrim4028
    @speedeetrim4028 7 หลายเดือนก่อน

    boost on a 302...Cometic MLS gaskets machined flat heads & ARP studs...or do it wrong a few times & learn...been there done that...Im running 15#s boost on a turbo set up stock block...no pro here just what works

    • @TheInfamousProject
      @TheInfamousProject  7 หลายเดือนก่อน

      I hear ya. We're talking a mere 5lbs here lol

    • @speedeetrim4028
      @speedeetrim4028 7 หลายเดือนก่อน +1

      @@TheInfamousProject you know you always want to turn it up 1

  • @lr7993
    @lr7993 7 หลายเดือนก่อน

    Ruff project. But I’m sure “neighbor around the corner” will appreciate it 😂😎

  • @truexkev2737
    @truexkev2737 7 หลายเดือนก่อน

    Nice work

  • @mustangjoe2066
    @mustangjoe2066 7 หลายเดือนก่อน

    Shellac 😎👍,works great

  • @bobfalfa76
    @bobfalfa76 7 หลายเดือนก่อน +1

    If it wasn't for their vehicles, I wouldn't be able to tell who the hell half the ppl I know are, lol.

  • @joey4872
    @joey4872 7 หลายเดือนก่อน

    Oh yeah the intake gasket slip! Been there. There is an assembly technique to prevent the gasket slip from happening. If anyone is interested? Just ask!

  • @nikreh5240
    @nikreh5240 6 หลายเดือนก่อน

    Speaking of black foxes, what happened to the 88' T-Top fox you were going to save?

    • @TheInfamousProject
      @TheInfamousProject  6 หลายเดือนก่อน +1

      It's in Canada... Need to get a title for it

  • @quinlanthomas240
    @quinlanthomas240 7 หลายเดือนก่อน

    Were you able to see where it was leaking on the old head gasket ?

    • @TheInfamousProject
      @TheInfamousProject  7 หลายเดือนก่อน

      No.. they were Mr Gasket brand with that tin foil shit on there everywhere.. I didn't even know people still used their products lol

  • @laurencerilling5873
    @laurencerilling5873 6 หลายเดือนก่อน

    They used crap head gaskets
    And the wrong intake gaskets
    Didnt glue the intake gaskets on
    Didnt use alignment studs
    Didnt move the bypass out of the way
    Didnt look in the holes
    Must have not smoked enough

  • @ckygogo
    @ckygogo 7 หลายเดือนก่อน

    Can you say ARP head studs?