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Jerry Motorsport
United Kingdom
เข้าร่วมเมื่อ 27 พ.ค. 2020
Following the journey returning to Motorsport for your host, Jerry, and charting the works required to the previously competed MG Midget and some other vehicles run by Jerry.
We'll be looking to get back into autotests and autosolo events with plenty of garage time too working on the cars. Hopefully I can also spend some time on track days and would like to give sprints and hillclimbs a go too.
Jerry Motorsport [JER-EE MOH-TER-SPAWRT]
We'll be looking to get back into autotests and autosolo events with plenty of garage time too working on the cars. Hopefully I can also spend some time on track days and would like to give sprints and hillclimbs a go too.
Jerry Motorsport [JER-EE MOH-TER-SPAWRT]
Stripping down the driver’s side suspension on the 1275 MG Midget
In this episode we strip-down the driver’s side suspension on our 1973 MkIII MG Midget and hope we remember all the pit-falls of the near-side.
This should have been a simple and quick strip-down, but some complications and work commitments mean this has taken six months to progress. Sorry for the wait everyone!
We find that one of the lower wishbone pivot point bolts is seized in position and drastic measures are ultimately employed to remove it..
Content of this episode:
0:00 - Introduction
2:42 - Getting started on the strip-down
5:10 - Removing the road spring (lowering the lower arm method)
5:54 - Removal of lower wishbone
6:55 - Problems with the pivot bolt
8:49 - Cutting out the seized pivot bolt
9:37 - Removing the worn Frontline upper suspension arm
10:20 - Last part (lower arm) out
10:46 - Outro
Thanks for watching and please give us like, if indeed to you did, which really helps the channel grow and leave any comments you may have to help us improve the channel or to let us know things you want to know about the car or see being done.
You can also follow us / contact us on Instagram at jereemohterspawrt
This should have been a simple and quick strip-down, but some complications and work commitments mean this has taken six months to progress. Sorry for the wait everyone!
We find that one of the lower wishbone pivot point bolts is seized in position and drastic measures are ultimately employed to remove it..
Content of this episode:
0:00 - Introduction
2:42 - Getting started on the strip-down
5:10 - Removing the road spring (lowering the lower arm method)
5:54 - Removal of lower wishbone
6:55 - Problems with the pivot bolt
8:49 - Cutting out the seized pivot bolt
9:37 - Removing the worn Frontline upper suspension arm
10:20 - Last part (lower arm) out
10:46 - Outro
Thanks for watching and please give us like, if indeed to you did, which really helps the channel grow and leave any comments you may have to help us improve the channel or to let us know things you want to know about the car or see being done.
You can also follow us / contact us on Instagram at jereemohterspawrt
มุมมอง: 1 710
วีดีโอ
Finally a Motorsport event for the channel - Shere Hill Climb 2021
มุมมอง 4483 ปีที่แล้ว
In this episode we down tools and take a trip to the Shere Hill Climb (sherehillclimb.co.uk) in our 1943 MG ND (Supercharged straight six) special model produced by the MG Car Company for use in motorsport events such as hill climbs. This was a fantastic day out watching and ultimately a multitude of cars from all sorts of manufactures with lots of history in the Paddock. Unfortunately, we foun...
New front brake calliper and brake bleed for the 1275 MG Midget
มุมมอง 3.7K3 ปีที่แล้ว
In this episode we fit the first new brake calliper on our 1973 MkIII MG Midget and install EBC Green Stuff brake pads. This should have just been a simple replacement, but slight differences in the casting results in us getting the grinder out to ‘make things fit’. We also rather annoyingly find out that new parts are not quite made to the required dimensions and we have to re-use the old pad ...
Upgrading to taper roller wheel bearings on front axle of the 1275 MG Midget
มุมมอง 6K3 ปีที่แล้ว
In this episode we fit the new tapered roller bearings to the front axles as an upgrade over the standard wheel bearings for our 1973 MkIII MG Midget. Taper roller bearing kit for MG Midget is an upgrade over the standard front hub bearings which are angular contact ball bearing type. These original bearings work well but does not allow for any adjustment as the bearings wear. Taper bearings pr...
Fitting new front suspension parts, including the Frontline Developments kit, to the 1275 MG Midget
มุมมอง 13K3 ปีที่แล้ว
In this episode we finally get the replacement lower wishbone fitted to our 1973 MkIII MG Midget. We also fit the new Frontline Developments front suspension kit to replace the very old and worn out kit along with SuperPro bushes to the lower arm and trunnion. Yet more Bilt Hamber products in this episode with the use of Dynax-S50 extreme duty anti-corrosion wax for cavities, voids and long ter...
Preparing the chassis (de-rusting) before re-fitting of the front suspension on the MG Midget
มุมมอง 2K3 ปีที่แล้ว
In this episode we remove the rust from near-side front wheel area of our 1973 MkIII MG Midget and prepare the area for re-fitting the suspension components back to the chassis. After removing the worst of the rust on the spring housing / upper arm mount and lower wishbone mounts with a drill mounted wire brush, we move on to treating with a rust removal compound (Bilt Hamber DEOX-GEL) to remov...
Cleaning the rust off the removed suspension components removed from the MG Midget
มุมมอง 8K3 ปีที่แล้ว
In this episode we take the suspension components taken from the near-side of our 1973 MkIII MG Midget and remove the rust. After de-greasing the components they were wire-brushed to remove significant rust and remaining paint and then sat in a rust removal solution (Bilt Hamber DEOX-C). As kingpin bushes could not be immersed in DEOX-C, the axle was de-rusted using Bilt Hamber’s DEOX-GEL which...
Removing the broken suspension components from the MG Midget
มุมมอง 4.5K3 ปีที่แล้ว
In this episode we finish taking the suspension apart on the 1973 MkIII MG Midget. Finally removing the lower wishbone, that was found to be cracked, and the upper arm, that has wear and was the source of the suspension banging noises. Attempts to remove the trunnion and kingpin from their respective arms don’t succeed; but the reluctant anti-roll bar linkage does eventually yield with some cyc...
Starting the replacement of the cracked MG Midget front suspension lower arm
มุมมอง 7K3 ปีที่แล้ว
In this episode we start taking the suspension apart on the 1973 MkIII MG Midget to replace the lower wishbone, that was found to be cracked. During investigations into the banging noises, road trials seemed to suggest that the exhaust was bashing the bottom of the car making the horrible banging noises. These investigations did also identify a crack to the A-arm at the chassis mounting bushes....
R56 Mini Cooper S Water Leak Located
มุมมอง 17K4 ปีที่แล้ว
In this episode we finally work out where the water has been leaking from the R56 Mini Cooper S (Gen 2 BMW Mini). After an unexplained drop in water a few months back, the problem returned with more regular loss of water from the system. Small wisps of steam lead to a radiator hose that passes very close to the six-speed Gertag gearbox on the Mini which over the 100,000 miles have been in conta...
Delayed - Not enough garage time; sorry no proper episode this week
มุมมอง 874 ปีที่แล้ว
Just a short video to essentially say sorry for not being able to put an full episode together this week. Been trying to find the source of the banging in the nearside front wheel area, but nothing conclusive yet.
Replacing the fresh air ducting to the MG Midget heater with quick overview of the system
มุมมอง 4.8K4 ปีที่แล้ว
In this episode we replace the broken plastic air ducting on the 1973 MkIII MG Midget and have a quick overview of the heater system. I trial the use of 100mm internal diameter aluminium foil conduit, normally used for domestic extraction, to replace the plastic duct that has broken beyond repair. Thanks for watching and please give us like, if indeed to you did, and leave any comments you may ...
Fixing burnt out brake lights on the R56 Mini and using dielectric grease to stop it corroding again
มุมมอง 8K4 ปีที่แล้ว
In this episode we fix the burnt-out brake light fitting / bulb holder on the R56 Mini Cooper S and investigate the use of dielectric grease to prevent it occurring again. After taking the rear light cluster out in order to get the old lamp holder out, we thoroughly clean up the metal contacts and apply dielectric grease to try and keep the area corrosion free. Corrosion build-up seems to cause...
Which is best to clean lightly rusted Chrome / Brightwork - Polish, Wire Wool or Aluminium Foil?
มุมมอง 3.5K4 ปีที่แล้ว
In this episode we look at different cleaning methods of brightening up slightly rusted chrome / brightwork on the 1973 MkIII MG Midget (and 1930 MG M-Type Midget). I investigate the use of aluminium foil, wire wool and good old-fashioned elbow grease to clean the brightwork on the midget. I then discover that not all steel wire wools are equal and discover that 0000 grade wire wool delivers ex...
Finally! a Fan Belt that fits the Midget and we get two horns working
มุมมอง 2.4K4 ปีที่แล้ว
In this episode we get back to the 1973 MkIII MG Midget and finally sort out the slipping fan-belt issues and fix the horns. The replacement for the sheared alternator pedestal arrives only to find the treads need some work before the nut will go on. Then it turns out I’ve probably had the wrong size fan belt on the car for some considerable time. Still a bit annoyed to find that the belt won’t...
Fixing the boot/tailgate switch on the Mini Cooper S Hatchback (R56) without wrecking rubber cover
มุมมอง 36K4 ปีที่แล้ว
Fixing the boot/tailgate switch on the Mini Cooper S Hatchback (R56) without wrecking rubber cover
Finally getting the Midget out for a shakedown drive (Fan Belt problems develop AGAIN!)
มุมมอง 3.8K4 ปีที่แล้ว
Finally getting the Midget out for a shakedown drive (Fan Belt problems develop AGAIN!)
Completing the changing of the MG Midget’s oils
มุมมอง 8K4 ปีที่แล้ว
Completing the changing of the MG Midget’s oils
Changing the MG Midget’s oils - plus I get a long over-due haircut
มุมมอง 5K4 ปีที่แล้ว
Changing the MG Midget’s oils - plus I get a long over-due haircut
Flushing the MG Midget’s cooling system
มุมมอง 12K4 ปีที่แล้ว
Flushing the MG Midget’s cooling system
Tabletop Rally (Navigator practice) in leiu of available motorsport sessions (No MG Midget)
มุมมอง 1374 ปีที่แล้ว
Tabletop Rally (Navigator practice) in leiu of available motorsport sessions (No MG Midget)
Checking the MG Midget against MOT inspection manual and investigating suspension and bumper issues
มุมมอง 4.2K4 ปีที่แล้ว
Checking the MG Midget against MOT inspection manual and investigating suspension and bumper issues
Getting the 1973 MKIII MG Midget back into Motorsport - Preparing the garage space first
มุมมอง 8114 ปีที่แล้ว
Getting the 1973 MKIII MG Midget back into Motorsport - Preparing the garage space first
Instructional laps of Donnington Park circuit
มุมมอง 3924 ปีที่แล้ว
Instructional laps of Donnington Park circuit
Prescott Hill Climb (School) with the SSC Stylus
มุมมอง 4094 ปีที่แล้ว
Prescott Hill Climb (School) with the SSC Stylus
MG Live 2010 Autotest - The one that broke the Midget's gearbox
มุมมอง 7344 ปีที่แล้ว
MG Live 2010 Autotest - The one that broke the Midget's gearbox
MGs on Track - Donnington Park Track Day 2012
มุมมอง 2054 ปีที่แล้ว
MGs on Track - Donnington Park Track Day 2012
My issue was the pin connector on bulb cluster, one pin shorted had to get new cluster and connector
Mine is back in the garage today for a water leak. Changed the water pump and didnt fix it so I have left the car with a tear in my eyes. Pending an update!
Two years after this video, I came back here because a buddy of mine from the MG Car Club (of Western NY Centre) can't make his brakes work on a Midget he acquired last year, and I needed to see a caliper mounting video. The master is fine, but he can't get the pedal to stay up, the pressure fails, and the brake fluid bleeds back into the master after pumping them. As in, pump, pump, pump x 10, hold pressure, pedal about half way down, brakes all seem to work, but then let off on the pedal and fluid comes back into the master and the pedal goes to the floor next time you pump it. Turns out, the front calipers are both on the wrong side, upside down! The bleeder is on the bottom! I'm sure the previous owner has never had brakes working, and that probably contributed to why he sold it. We'll flip them over tonight after work, and I'm confident the brakes will be fine.
Did the belt goes to crankshaft pully as well ?
Yes belt goes round crankshaft pulley, water pump and alternator (or dynamo if you have one)
Why on earth do you feel you have to put annoying music on at the same time as you are talking. It makes no sense and is just distracting.
Noted, thanks for watching Steve
Some time ago I got a dashboard warning message to say that I had a rear bumper left brake light failure on my 2017 Mini Cooper Clubman. Well, thakfully it wasn't a blown bulb (£39.99!) so I simply cleaned the terminals, gave things a jiggle and we were soon back in business. However, last week I got the same message. Once again it wasn't the bulb, but I noticed that one of the terminal plates inside the light assembly had partially burnt through. I simply refuse to spend £100 on a replacement tail light assembly, so I cleaned up the electrode, repaired the defect using a blob of solder and smeared some Copper Ease grease onto both electrodes (I didn't have any dielectric grease) before reassembly. It seems that the lights on various Mini models must be prone to moisture ingress, so Mini/BMW could do well to apply some dielectric grease to all terminals during initial assembly. Thanks for your clear video clip, Jerry.
The front fog lights/ side lights are notoriously bad for getting moisture in them. Rear clusters less so but clearly something upsets the status quo. Glad you found this a useful video!
Thank you! I am going to look for my first ever british sports car on next sunday. A 1968 MG Midget. Hopefully the car is as good as the seller says, maybe I drive home on sunday with a new hobby. This video was nice information on the regular maintenance. Subbed.
Glad you found the video helpful. I hope the car you are going to see turns out to be a good example and it signifies the beginning of an adventure!
Hello Jerry, how's the midget going just found your channel and enjoying the mg videos. Looking to buy a mk3 myself so very interesting.
Hi thanks for watching. Midget was going great last time she drove but I need to get back into the garage and get back into some competition. Unfortunately life took over a bit and my PC had a disastrous crash and I lost a lot of data. Hope to get some more updates soon.
Are you sure it’s not German made? It seems to respond only to force.
😮. Thanks for watching 😊
Thank you Jerry very good useful information
Glad you found it useful. Thanks for watching
Great video thanks, just about to do this on our Cooper D.
Are those mgb calipers?
They should be the base Midget ones; as that was what I ordered 😊. They are 95% identical to the original Lucas units with the colour and the minor casting difference, that needed modification, being the only differences.
Timeless video I have a bugye with the same setup. My brake system is with the mgb calipers and spitfire rotors. It's not a simple bolt on, but after working out some issues, I'm happy
I’d like better brakes but would need to check the rules for the historic class I enter competition in. Not bad with the servo assist but would be good to have more longevity before getting too hot.
I froze the race to aid in seating.
That’s a good idea to make life easier. I did consider heating the hub.
You mean coolant
Yes I probably should have titled the video coolant leak located 😂
Indeed I should have been more accurate there 😉
Hi well after watching the tutorial for the switch removal I decided to have a go soldering iron and switch in hand The result is a FAIL couldn’t get the old switch out the circuit board No matter how much heat I applied seems so tight So it’s now back on the car still not working Any advice hints ? Thanks
Hi sorry missed your comment. I seem to recall there may have been some tabs soldered in. Unfortunately I’ve not got the car anymore so can’t verify. Thanks for watching
Thanks, Jerry. That threw some light on my not entirely tight fan belt. Before watching, I ignored the adjusting screw as a possibility on the grounds that no manufacturer could possibly put it somewhere so hard to get to.
It’s a mystery. It’s almost like they didn’t thing the belt would need maintenance. Thanks for watching!
This was an absolutely great video really has been so helpful 🙏
Thanks for watching and thanks for the feedback!
Hey, Jerry - Just watched this today, and I do have a question - the pads really go in "dry" like that? I would have assumed that you needed grease on the edges where they ride in the caliper. Just curious!
Haven’t found the need to grease this area but I guess no harm in doing it if you are worried about the pads catching
3:47 😂😂
Made me smile in the edit 😁
The oil filter paint had me laughing 😂 I know that sort of stuff happens to me!!
I felt such an idiot but I wanted to share my journey (good and bad) to show it is not at all perfect and maybe entertain and educate along the way 👍
Not clear what, how you connected the garden hose.
Pretty sure I just shoved it in one of the radiator hoses. Thanks for watching
Where did you get that "groovy" roll bar?
Hi, sorry for the late reply. It came from Moss I believe (before my time with the car)
Use the aluminium Brillo pads, that stops you scraping the rust particles as abrasive paste all over your chrome. Soak the whole thing in WD40 for a week before you start as it softens the rust.
Thanks for the tip! Thanks for watching
Great to see real world mechanic-ing rusty bits, bent bits etc., well done.
Thanks for watching 😁
Jerry, I’m aware it’s a couple of years since fitting the horns but do you remember where you purchased them. Was it Moss or MGOC club shop. Thanks
Sorry just seen this comment 😬. Horns came from Moss
Any update on the fix? Still holding strong?
Ah sorry missed your question. Unfortunately due to unexpected circumstances I no longer have the Cooper S but we do have a same Gen Mini One so keeping an eye on the issue with that car.
Just doing this now. This kind of build is something that needs to be addressed under EU right to repair law. That plastic weld should be replaced by 2 self tappers.
Now Jerry obviously better than my 64 Midget as you're smiling even before you get behind the wheel 😂. Excellent hopefully head gasket now all sorted and onwards and upwards for your next event. All the very best Johnny 👍
Head gasket now sorted but we found the rigs were broken on two cylinders and then after getting it all back together we had some terrible big end noises. Currently replacing the big ends and mains 😬
Does the Frontline suspension require greasing every so often? I am working on a 1970 mgb gt mk3 and am thinking about the conversion for ease of maintenance.
Hi Duncan, the version I purchased of the front suspension kit has aircraft style bearings (forget the fancy name for the type) which do not require a regular grease application. In fact the instructions make it very clear to apply NOTHING to these bearings. The version of the arm I was replacing had no grease nipple which was odd so must have been pre the addition of grease nipples. Frontline said that they were making the change to the (fit and forget) aircraft bearings as people didn't grease the joint and the arms would wear out. I assume they have also moved to these bearings on their other kits. Good luck with your MGB.
Trying to replace my front bearing with tapered roller bearings, but when I put in the new races, the front one all the way seated could be spun in place by hand. Any suggestions on how to fix this without buying a new hub?
Oh that's not an easy one. Are the new bearings too small (relative to spec) / same as old ones? If they differ from the old ones you could have a badly machined bearing. If it is the same size as the old all I can think of is that the bearing has been loose previously. Whilst you can rotate it by hand, does it feel loose in the hub (i.e. up and down / side to side)? How easy is it to move? It might be snug enough to torque up and not be an issue, but as I'm not a mechanic by trade, and I haven't seen it for myself, I'm not really going to be offer you your best solution. Sorry; I suggest you ask a local garage for their thoughts perhaps? Good luck.
@@JerryMotorsport I got them from Moss Motors that are supposed to work for 1972 MG Midgets w/Wire wheels - kit part# 125-822. Not sure the size - but I have tried both of them in the kit and they both can be moved by hand - spin and up and down and feel about the same looseness. I will have to search and see what size they are supposed to be. Thanks for the help and I will let you know what I do and the suggestions I get.
I used a punch around the inner surface of the hub surface and used loctite bearing surface 660. Worked great.
Hi Jerry, any new videos coming please? Missed the regular updates. 👍
Hi Lee, thanks. Yes I'm hoping to get more videos out but my desktop computer had a melt-down (Blue screen of death) and I'm using a laptop to re-do what I had. Thanks for your support and patience.
Thanks Jerry, sorry to hear about the computer, hope it gets sorted. Look forward to the new vids. Perhaps you could do a history segment on how you come to own your 70's Midget and why it ended (apparently) laid-up in the garage for a time. I have issues starting mine whenever it's stood for anything longer than a week, fuel pump struggles to get fuel from tank to carbs, perhaps you could do an episode related to fuel pump, etc? Mine's a 1978 model so differs from yours but would still be good to see. Also handbrake cable replacement/adjustment, etc, etc. Thanks.
Lee, I'm hoping to be doing an update video shortly on what has been going on since the last video. I was thinking about some history on 'Midge' as part of a 'trailer' for the channel. However I'm incredibly busy with my day job (not a mechanic) at the moment; again something I was planning to put into a trailer.
Good news Jerry, I'll look forward to seeing the next updates. Cheers, Lee.
I spray mine with maintenance oil and gently polish it.
Yes I thing an oil would be good to help keep rust at bay a bit longer
Who supplied the brake parts that did not fit?
Hi, I would have to check my invoices; I had parts coming from various suppliers. Oddly the driver’s side had the correct flat spot and I didn’t have to get the grinder out.
I’d change the grub screw in the top arm to a bolt if you can as they seize in no time. Maybe a large dose of wax would help too
Thanks Mark, that's not a bad idea. Area did get a good dose of wax and I think I had copper grease in there too. Old ones were replaced so I never tried to take the old ones out. Thanks for watching!
Thanks, great video! Did my trunk release, works well.
Glad it worked; thanks for watching and leaving a comment.
Thanks so much for this! We had the same problem, actually got an MOT failure which wasn't expected (no other garage has failed it on that before) I used a heat gun like you suggested. I dabble in electronics so actually had a suitable microswitch knocking around. I used solvent weld (like for PVC plumbing) as I don't have a glue gun. which did an okay job in re-attaching the lid. It was a little uneven where I had pried it off so also added some silicone sealant around the perimeter after welding. Let's see how long it lasts - the rubber 'button' actually has a split in it so it's not super weatherproof from the bottom up.
Glad this was a helpful video and has saved you from a costly replacement part. Thanks for watching and commenting
Take a drink everytime he says dielectric grease
😂
@@JerryMotorsport 😁😁😁
Why did you get rid of the anti roll bar?
In this episode I removed the anti-roll bar to clean up and repaint the anti-roll bar and upgrade the mounting bushes to polly. I also found out that the old bushes were the original size but the bar is actually a thicker one (from an MGB I think; 5/8"?? from memory). Coupled with the upgraded suspension arms this really helps with the handling. The roll bar went back on as part of fitting the new suspension to the driver's side.
@@JerryMotorsport Thanks for your time.
Hi Jerry. I know this was not about your suspension but I am thinking of purchasing the same suspension kit as you, wounding if you think this is a worthwhile upgrade over replacing the original dampers?
Hi, thanks for watching and commenting. To be honest I've not driven a car with the standard dampers; our car came with what must have been the original frontine upgraded front arms. What I can say is that after completing the installation and competing with the car recently, it has great turn-in and almost no understeer. This setup is certainly stiffer than the single arm of the original damper and the modern AVO adjustable dampers give an excellent ride. Worth the investment IMHO.
Thanks, Jerry. I can't tell you how much I appreciate these videos. I've referred to many of them for my Midget, and keep referring back to them over time for additional maintenance. But the key is that I watch them as they come out because they're educational and entertaining, and they're well filmed. So thanks again!
That’s fantastic to hear. So glad the videos are proving useful. I’m hoping to be stripping down the rear suspension over the winter and perhaps some work on the fuel system. Do let me know if there is something you would like to see me do; it’s always good to have content ideas!
@@JerryMotorsport lubrication points, rear suspension is a good one, I just did the leaf spring bushes and put fresh oil in my rear dampeners. But need to completely disassemble the rear at some point. New gasket on the differential. Bearings. Transmission oil.
I added this kit to my 61 bugeye with mgb calipers and spitfire rotors kit
The Frontline suspension kit is good. I'd like to get their big brake upgrade and potentially do the rear disc conversion too. Down side it might put me in a different class for my competitions. Thanks for watching!
I have a bugeye sprite with the same setup for the shocks and suspension Spitfire rotors, mgb calipers for the brakes The rear has ssbc vented rotors The tie rod ends hit the rotors at full lock. Fixed that by adding split collars to the rack under the boots. I have a sbc 383ci in the car and a th350 I'll try a more aggressive brake pad
Caly your bugeye sounds like fun with a 383ci. Thanks for watching!
Hope I can find a european sounding horn at my local parts house. My horns are dreadfully inadequate.
Good luck with sourcing the sound you are looking for Mike. Out of interest are these new horns of mine that European sound? I thought they sounded rather more modern than I was expecting.
Fan belt good, alternator loose. Its not a great system. Anyone know of a tensioner pulley setup for these cars?
Hi Mike, thanks for watching and an excellent question. I wondered many times when doing this fanbelt work if there was a tensioner system available; I'm not aware of one. Perhaps I should look at fashioning one; although I'd have to be careful not to put excessive load on the pullies and create other problems. In fairness, it has been much better since sorting it out and just one of those things that us classic car owners need to keep a check on. All the best..
Hi Jerry, great video, my problem is the weather shield has corroded away and need to replace that, do you know if it's possible or do I need to replace the whole thing? I can see weather shield replacements for sale online but I can't see a join with the original one I have currently fitted....any help would be great. Thanks.
Thanks for watching and commenting. I think the rubber weather shield comes as part of that rear light unit and not something readily replaced. You might be able to remove what is there and fix in a sheet of rubber (old inner tube perhaps?). I saw a few videos removing this rubber to get to the damaged switch behind. This is why I did my repair the way I did mine as I wasn’t confident to get a good replacement rubber put back. Good luck with yours if you go that route.
@@JerryMotorsport thanks for the reply Jerry, I've bought one on ebay, I think I'll need to cut the old rubber out and push the new into place, a weekend job I think!
Not enough prep work on removing the rust before treatment. Also deox c gel should be covered with cling film and left for 24hrs min. This process should be carried out more than once if rust is still present, to eradicate effectively. Apologies if I sound negative or nitt picky but wouldn't want to see the rust reappear any time soon 👍
Thanks for the tips. Not got on very well with the gel. The other side went much better and any remaining rust was treated with Hydrate80.
@@JerryMotorsport hope I didn't sound to moany Jerry as I do enjoy watching your videos but I'm becoming bit of an expert with rust treatment as I work on old Fords 😆
@@JerryMotorsport think the reason why you're struggling with the gel is that it's not supposed to dry out..the clingfilm helps let it "simmer" on the rust. after 24 hrs pull the clingfilm off and the gel "should" be washable. I'm looking at Bilt for my Z3...so it should be interesting!
Now I can see what’s happening on the backside. It tells the whole story. You can see the mess. 😆
It’s not great is it. Hope you get it sorted out.
Thanks Jerry. Super helpful.
Thanks for watching, glad it was helpful!
Jerry... are you flushing the heater-core? If so, where is the out flow and is the heater valve opened?
Hi, yes I flushed the heater core as well as the main cooling system. The isolation valve is curently stuck in the open position so when I added the flushing chemical it would have gone around the heater matrix too. At 7:51 you can see I've disconnected the hose from the heater isolation valve to fush through fresh water to make sure I got as much cleared as possible from the heater. Ideally I would have used the other hose (upper from the core) and flushed in the opposite direction to normal flow; this was just easier to remove the hose from the valve.