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project ram life
เข้าร่วมเมื่อ 31 ต.ค. 2016
Uploading ram 2nd gen cummins content mainly!
And a little bit of everything else in life.
And a little bit of everything else in life.
วีดีโอ
dodge 2nd gen diesel lock and un lock torque converter surging issue update!
มุมมอง 15Kปีที่แล้ว
dodge 2nd gen diesel lock and un lock torque converter surging issue update!
98 cummins putting together rotor and wheel bearing .
มุมมอง 75ปีที่แล้ว
98 cummins putting together rotor and wheel bearing .
98 dodge cummins drivers side front brake hose removal.
มุมมอง 78ปีที่แล้ว
98 dodge cummins drivers side front brake hose removal.
ram cummins 2nd gen rotor and wheel bearing separation.
มุมมอง 267ปีที่แล้ว
ram cummins 2nd gen rotor and wheel bearing separation.
98 cummins dodge torque converter lock un lock issue.
มุมมอง 347ปีที่แล้ว
98 cummins dodge torque converter lock un lock issue.
2nd gen ram cummins surging transmission lock unlock torque converter.
มุมมอง 14K2 ปีที่แล้ว
2nd gen ram cummins surging transmission lock unlock torque converter.
ram 2500 2nd gen dana 60 Front differential shaft seal
มุมมอง 4.5K2 ปีที่แล้ว
ram 2500 2nd gen dana 60 Front differential shaft seal
Mine was neg cable off alternator at block
U saved my ass. Man Ive been so fucked for so long. All this money spent. And finally it works. Thank you so fucking much
@@tannerhooper7211 I'm glad I was able to help!
That engine has a Wonderfully distinctive sound!😍
I just lost my dad a few days ago. Im trying to fix his dodge (2001) in order to haul our cattle and sheep to market. Had our current issue (not the one described here, tpps, and map sensor i think? Basically erratic acceleration..but problem keeps morphing on me... anyways) bring me here. I like your style! Ima sub! And check out what other wonderful bits of knowledge you have! My dad wouldve pissed about the transmission rebuild, but glad the issue got sorted! Wish i found your vid sooner! Ill definitely try this once i get my current issue figured out! Please make more vids on your dodge if you can; this my dads last truck, he bought it new. It was special to him as 1st he could ever get that way. So its special to me now! And i wanna treat it right!
Also, my uncle, used to be an electrician, and he was known for getting rid of superfluous nonsense in controls! (not in automotive field, DC magnet controllers and hydraulic control relays) so I can Respect removing nonsense!😅🫡
14:15 i think the people that suggest running the ground to the battery in that situation, probably live up north. These dodges can rust bad! And grounding is sooo important! That i wouldnt really trust solely the frame work for it😅
17:40 that coincides with the dodges having rust issues and not good grounds. Good tip!
Yo! Same! Had transmission rebuilt and issue reappears later!
This isn't my current issue, I still have this problem randomly, but was looking for a solution to another problem. Glad I found this tho!
The auto trans is the defect from Dodge
Mine is fine and it’s got nearly 200k on it. Probably just depends on the user.
Are the black wieres from the tcm have orange line?
is this compatable with a 04 cummins? i hate this surging issue
Can I pay you to do it ?
I'm sorry if this is a dumb question but does this problem also occur for 12v engines?
Yes. My 12 valve same issue and has an 8k rebuilt trans
Having this issue with a 2003/3 GEN will this work don’t see any connector plug need help
same here for a 04 having the same issue
Thanks for the video man. Helped a lot
This absolutely took care of my 3-4 lock/unlock issue after 2 years of fighting the same battle. Thanks for this, wish I would have run across this sooner.
I developed severe hunting especially in cruise control which would clear if I drove over 70 mph. Replaced the Governor Pressure Sensor 12415C and Governor Pressure Solenoid 12432A solved the problem. But still fighting the other minor hunting issue as it did not go away.. Relocated the ground wire that runs along the alternator did not help Installed the APPS Noise Isolator Dodge 5.9L 1994-2004 from BD Diesel did not solve the problem. Replaced the TPS (throttle position sensor) thinking there could be a dead spot in sensor did not help. Problem solved when I cleaned all the ground cables from the battery to the firewall. At that firewall point there is a ground strap that goes to the PCM. Cleaned all those eliminated the problem. They were all badly corroded. I have a 5.9 2002 2 wheel drive so I guess that would come as no surprise.
outstanding
could you show detail behind cover and how the tension is adjusted?
Did you cut each 4 wires on the driver's side and plumb them all Into one wire and then ground it to the drivers side battery or did you cut it before it switches to 4 Individual wires then you just grounded the single line before it splits off into 4 lines into the drives side battery. That's what I'm confused about thanks.
What is that sensor itself called
Hey bud good video, but I'm still a little unsure, especially on the splicing part of the wires going to PCM. help me
I did all those tricks and installed a tcc lockup switch !
How do you fill the fork compartment back with gear oil? Do you just fill from diff cover?
Is this only common for a 24v ?
Thank you!!! I’ve owned my 2001 for 5 years and tried several recommendations. I just eliminated those plugs and now on i10 tirando HUMO!!! THANKYOU again from AZ . PURO HD!!!
Arriba Mexico, Cabron Gracias
But this is a great video thank you. My trucks been doing the same thing for two years and I finally just bought the manual transmission. I’m over the automatic, but this is nice to know. Thank you.
Or you could just do what I did and pull the stupid automatic transmission out and swap it over with an envy 4500 cured the problem got me is decent news transmission for four-wheel-drive for 2500 bucks. Problem solved.
I just talked to a diesel mechanic that has been working for a dodge dealership for a long time. Yes this was a bad issue with 2nd gen automatic trucks. The wire plug in on that ground coming from ECM to PCM is the problem. He told me what’s happening is that the plug in gets hot and interferes with the pcm causing the torque converter to lock and unlock rapidly. He quaranteed by cutting out this plug and grounding each end of the wire to the batteries has and will fix the problem!!! He also said you can sotter the 2 wires together once the plug is removed. Either way works!!
Interesting. Everybody else has said it's a bad alternator giving off ac voltage interference to that wire that runs over the alternator.
@@CaseyDevillier tried cutting the plugs out and it didn't solve the problem either.
I just bought a 2002 24V a few months ago. Truck is great but having the same issue!!! I changed the throttle position sensor, no luck! Re routed the ground wire, no luck! I will try this and hopefully it fixes the problem!! The truck is a great truck hopefully this fixes this aggregating problem. Cause when it starts acting up it’s pretty much non drivable!
Hopefully this takes care of your problem.
I did all this today with my wiring… it didn’t fix the bucking
Does it start at a certain speed ? And have you done any other things to the truck besides what you have said in your first comment?
Yes. I rerouted the wire first. It didn’t fix the problem then today I cut the plug off of the ground and grounded each end separately and it didn’t fix the problem. Yes it only does it at 50 mph and over also sometimes it takes several miles of traveling before it starts doing it. Once it starts jerking back and forth my tachometer starts surging up and down. I know it’s not the transmission because I had it tested. Also I grounded the pcm that’s located on the firewall, to the battery as well.
Does it do it from a cold start or only after driving at temp for awhile. If it does it from cold your pcm may already be to damaged. Swap it out for a known good one as a test if possible.
How did you pop the old seal out?
I used the all tread from the wheelhub side with a hammer tap on all sides became lose enough to pull out from the 4x4 fork opening. Hope that helps .
Dude. I just bought a 24v today. I started having this issue on my way home from buying it. I did not notice it on the test drive. I really thought I was about to have to rebuild my trans. I hope this will fix my issue. Thanks for the knowledge brother
Did this fix your problem???
Did this fix your issue??
Man you are persistent brudda!! I have a 99 2500 and I KNOW your pain minus the trans rebuild, new pcm except. I got lucky with the BD wire diode fix plus I did some extra ground support wires especially to the area around the pcm. I know exactly what you mean by the curse coming BACK! Thank you for the explanation and sharing your experience!
th-cam.com/video/myHsbxU_K8w/w-d-xo.htmlsi=Yz4EEVswzmiULu_I
So I’ve heard of using a tps delete would that work also?
To be honest I haven't tired that . But just thinking I'd say no because it's a ground ac noise interference issues. I tried just about everything and since I did what I explained in the video haven't came back or given me any problems . Running strong . Hope this helps .
@@projectramlife819 look it up because guys are using it for the same reason and what it does is hooks up to the tps clip and you set where you want it to shift manually it tells it when to shift and I feel it’s the same thing because that comes from the module to the tps and that tells when to switch and with the issues the tps isn’t sending the right info to the module because it’s getting interference because of the alternator
@@HorizonnetworksccI believe that was only for the common rail trucks
Was it surging when you where driving, like for me about half throttle 2,3, and 4th gear will do it recently
Yes it was , around 40 to 55 mpg would lock ans unlock really bad .
For anyone about to do this, no need to splice anything. Just cut the one coming from the drivers side just long enough to reach the battery on that side. And cut the other one right at the plug near the battery, reGround it and you’re good to go. Appreciate the video definitely fixed the problem and didn’t even have to splice anything 👍🏻
Was this a total fix for your problem??
@@CaseyDevillier yes it drove from 336k to 365k issue completely gone… transmission just went out tho, nothing to do with this I just drove the truck really hard. Putting a built trans in it gonna see how far it’ll go
Did this issue cause your truck to not shift into overdrive at all? I got a 99 24 valve
@@mitchelllawrentz766 no just didn’t want to coast at any speed by the end of it but it started the surging at 45
@@mitchelllawrentz766 I don’t think so but I didn’t drive it fast like that. Drove it for like 3k miles with the surge and the trans took a shit after about 30k once i fixed it. Got a built roadripper in it now.
What wire you just said four wires in the front of the motor splice like a little bit more explanation on that thank you
Yes, it's the wire that runs from the right side all the way to the left side behind the alternative. From the ecm, it comes out as 4 and then becomes 1 wire . You can splice from where it's 1 and from there on the right side conect to negative post on battery terminal. Hope this helps.
Gonna try this tomorrow. My brand new converter is surging like crazy and driving me insane. Hopefully this does it tried everything else at this point 😂
Yes I was in the same situation. 🤞🏽 hope this take care of your problems.
What codes where you getting ?
I don't remember off the top of my head. But I was not getting any check engine light. Only if I scanned it it would give me a code .
Can’t find that wire on my 97 12v
Witch wire ? It might not be the same since it's a 12v more then likely that's why. The one in the video is 24v the 12v doesn't have all the electronics it's more mechanical.
What worked for me is very simple. Give it a shot all you guys what have this issue. I've tried all those little tricks, none of it really worked. What did the trick is completely rerouting that ground wire that he is taking about. Away from alternator and the block. I routed it over the top of the radiator right next to positive cable all the way too the battery. It is just long enough, you don't need to cut and extend it. Tru that first before cutting anything. If yall want me to make a video showing what I did, let me know. It's very simple, every 2nd gen cummins should do this.
Mine is definitely not long enough without an extension. Its already tight and i cant even move it up 5 inches
th-cam.com/video/myHsbxU_K8w/w-d-xo.htmlsi=Yz4EEVswzmiULu_I
would love to see your simple solution, and video as well, his video is confusing to me. he made it after his repair and i dont see it well. Showing a piece of wire that was removed and flopping everywhere , i dont get it
@@JustPlaneMike th-cam.com/video/myHsbxU_K8w/w-d-xo.htmlsi=SoXeRbqi3sygGs5U
I did that and it didn’t fix my problem
Esa troca esta quedando chingona primo. Donde compro los asientos
Son los de la troca . No mas que los mande a tapizar.
would what you talking about work for a 95 dodge with the 12 valve cummins. im having a problem with it not wanting to lock in overdrive
Me too
tps needs cleaned
Did you get this sorted
Could you slide that shift collar off that inside axle shaft with that axle out if you needed to replace it?
Yes you could .
Thank you, I’m gonna try this. Not waiting 4 days for the tool to come in
One main problem I have seen with all makes of Diesel trucks are young guys treating them like a race car. Diesels are to be treated with respect. They are made to work not hot rod. Somewhere these manufacturers have data on this. Of course they won't share it because they will lose money on sales. This cannot be honestly refuted with honesty.
Nothing burger?
how is your truck running afterward? I am currently having this problem and hopefully after my injection pump gets replaced for the second time it will stop the issue, It did it for the first time but shortly after a while it started again.
Yes indeed my truck did the same thing. It seems to be fine and then it would come back and do it again. But as of right now it's been working great haven't had the problem come back. Hopefully your is fixed after that .
HEY BROTHER I'M GOT IT (TPS) IT WAS THE PROBLEM NOW IT'S WORKING SUUUPPPERRRR GOOD.
Always great to find and fix the problem. Keep the 2nd gen Rollin 👍🏼👌🏼
IS THIS GOOD TOO FOR MANUAL TRANSMISSION??
I'm don't think that it will work for manuel.