BIG Mistakes Trying to Fix a Vacuum Leak on My EdelBrock Pro Flow 4 // Off the Leash

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  • เผยแพร่เมื่อ 28 พ.ย. 2024

ความคิดเห็น • 29

  • @wildhorses4x4
    @wildhorses4x4  2 ปีที่แล้ว +1

    Comment below what you think my big mistake was in the end: WRONG ANSWERS ONLY😂

    • @nicktaylor9957
      @nicktaylor9957 2 ปีที่แล้ว +1

      Supply and return fuel lines switched?

    • @lemos359
      @lemos359 2 ปีที่แล้ว +1

      Loose connection on the battery ?

    • @porkfist4737
      @porkfist4737 2 ปีที่แล้ว +1

      Reversed polarity of the alternator valve

    • @nickefgen9219
      @nickefgen9219 2 ปีที่แล้ว +1

      You forgot to hook up the exhaust bearings

    • @Stangherbie1234
      @Stangherbie1234 2 ปีที่แล้ว +2

      Capacitor was low on plutonium.

  • @timdco
    @timdco 2 ปีที่แล้ว +8

    you had the firing order on the plug wires wrong?

    • @hansoor8719
      @hansoor8719 2 ปีที่แล้ว +2

      My guess as well

    • @wildhorses4x4
      @wildhorses4x4  2 ปีที่แล้ว +3

      Unfortunately...... yes

    • @GaryH-pw9cm
      @GaryH-pw9cm ปีที่แล้ว

      @@wildhorses4x4 Old 312 Ford engines would run with four bad plug wires. Did not have much power but would idle just fine.

  • @iddddaduncan
    @iddddaduncan 2 ปีที่แล้ว +2

    How does this channel only have 13k subs, videos are great!

    • @wildhorses4x4
      @wildhorses4x4  2 ปีที่แล้ว +1

      Thank you! I appreciate that!

  • @GaryH-pw9cm
    @GaryH-pw9cm ปีที่แล้ว

    I had a rebuilt 351W that had an Edelbrock performer manifold. There was a vacuum leak on 7 and 8. No matter what I did 7 and 8 would leak. Thought it was the manifold, but it turned out either the block or heads were machined wrong causing a gap in the gasket. Replaced the engine with a different engine and used the same manifold and it worked fine.

    • @wildhorses4x4
      @wildhorses4x4  ปีที่แล้ว

      That’s such a hurdle to have to leap especially when you’re trying every other possibility. Nobody wants a bad block

  • @welndmn
    @welndmn 2 ปีที่แล้ว +1

    Secret torque sequence unlocked!

  • @TheMoldyOne
    @TheMoldyOne 2 ปีที่แล้ว +1

    I personally had to reset the computer and redo base timing. Started up perfectly. But I also got my timing set before I started it to 12 degrees

  • @Formerjughead
    @Formerjughead 2 ปีที่แล้ว +1

    They call it the "Number One Cylinder" for a reason. When I replaced my intake gasket I managed to burn my coil up.

  • @ChrisDaubitz
    @ChrisDaubitz ปีที่แล้ว +1

    Having the same issue can you please let us know what it was?

  • @BDGumby007
    @BDGumby007 2 ปีที่แล้ว +1

    If you've never ran out of gas? Do you even "Bronco" Bro!!? 😉🤣🤣😎❤️‍🔥❤️‍🔥🤟😜🤟

  • @chevyjohn7740
    @chevyjohn7740 ปีที่แล้ว

    What was wrong mine is doing same thing

  • @ryansearlybronco
    @ryansearlybronco 2 ปีที่แล้ว +1

    Why did you choose the pro flow over the sniper?

    • @wildhorses4x4
      @wildhorses4x4  2 ปีที่แล้ว +1

      When we did the engine swap in the Pitbull, the Proflow was kind of new so we wanted to test it out for ourselves and see how it did. I had the sniper on the old engine and never had a problem with it.

    • @jackieliner3812
      @jackieliner3812 2 ปีที่แล้ว +1

      Probably cause the proflo4 is MPI, more modern than throttle body.

    • @morganpowell2999
      @morganpowell2999 ปีที่แล้ว +2

      And less reported issues, sniper has a lot of problems with RF because the ECU is mounted on the unit.

  • @davidbrady9686
    @davidbrady9686 2 ปีที่แล้ว +1

    In todays world total transparency is needed…what happened?

    • @wildhorses4x4
      @wildhorses4x4  2 ปีที่แล้ว +1

      😅 Tim Collord nailed it.... firing order on the plug wires wrong

  • @arthuryoung8007
    @arthuryoung8007 6 หลายเดือนก่อน

    Didn’t even tell what the problem was.Geez😒

  • @jackieliner3812
    @jackieliner3812 2 ปีที่แล้ว +1

    The disturbtor needs to be set at 12*the ecm will do the rest of the timing