CCS | Failed Liner Removal

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  • เผยแพร่เมื่อ 2 ส.ค. 2022
  • The task of the CCS crew was to remove a failed liner using a robot water blaster. When the robot became lodged in the failed liner, it was time to call in professional divers to dislodge the robot - and remove the liner. The pipe was 21" RCP at a depth of 12' and 16' feet up the line.

    As always, safety was our number one concern.

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