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Kevin's Fix-it or Make-it Shop
United States
เข้าร่วมเมื่อ 13 ก.ค. 2016
Fix-It or Make-it projects, Homemade tools, Toyota FJ40 Landcruiser repairs.
Toyota Landcruiser Fj40 Fuel Pump Retro Mod Makeover.
I took newer style Toyota FJ40 fuel pump and modified it to have the features of the original early fuel pumps with serviceable valves and manual priming.
มุมมอง: 42
วีดีโอ
Drill Press Homemade Upgrade-Precision Spindle/Milling Head control.
มุมมอง 4.4Kหลายเดือนก่อน
I turned my vintage drill press into milling machine by making a precision spindle height attachment.
Homemade upgrade to a budget Cross Slide Vise for a drill press.
มุมมอง 169หลายเดือนก่อน
Bought a budget Cross Slide Vise and it had some play in both axis. I made some simple shims that increased its accuracy remarkably.
Homemade self-cleaning filter for ditch/lake pump intake.
มุมมอง 57หลายเดือนก่อน
I built an intake filter on my ditch that automatically cleans itself by using an internal rotating sprinkler. Could be used on a lake or other pump intake filter needs.
Trash to Treasure-Ryobi Circular Saw
มุมมอง 3512 หลายเดือนก่อน
I found a Ryobi Circular Saw in someone's trash. I was able to fix by making a a small homemade part.
Trash to Treasure- Ryobi Hedge Trimmer
มุมมอง 1832 หลายเดือนก่อน
I found a Ryobi Hedge Trimmer in someone's trash and repaired it and adapted it to use a Dewalt 20 volt battery.
Trash to Treasure Dyson Animal Vacuum
มุมมอง 502 หลายเดือนก่อน
I found a Dyson Animal Vacuum in someone's trash, it was easily repaired by finding a clog in it.
Rescued and Repaired DYSON VACUUM sucks up 40 pounds of bricks!
มุมมอง 893 หลายเดือนก่อน
I rescued this vacuum from the trash and repaired it and wanted to come up with a way to show how powerful it is, so I made a vacuum actuator to see how much weight it would lift. Its a beast!
Homemade Power Tool Stand from a shipping crate.
มุมมอง 2784 หลายเดือนก่อน
Homemade Power Tool Stand made from a metal shipping crate dug out of the trash. I mounted a Vintage Wet Grinder on top and fabricated a motor mount and tension system.
Homemade Electric Lift is a back saver!
มุมมอง 9674 หลายเดือนก่อน
Homemade electric lift that attaches to a ladder and easily lifts 4' x 8' sheets of plywood up to my the roof of my shed project. Uses a 1/2" electric drill to power a simple worm drive winch.
66 Year Old Radial Arm Saw with Homemade upgrades still can Cut It!
มุมมอง 7234 หลายเดือนก่อน
Vintage 1958 Craftsman Radial Arm Saw with homemade upgrades to make it easier and safer to use. Video Tour of the saw and some of the original accessories. Incredible construction by today's standards for a power tool.
Vintage Drill Press Homemade Upgrades
มุมมอง 11K4 หลายเดือนก่อน
Vintage Drill Press, homemade upgrades to make it easier and and safer to use.
Homemade wood auger bit rack made out of lawn edging.
มุมมอง 3264 หลายเดือนก่อน
I made a wood auger bit rack to organize and hang my bits on pegboard. I used some left over lawn edging as the material to build the rack. It can be used to hold bits on pegboard or this rack can sit on bench.
Restoring 100 year old Engine Hit and Can't Miss!
มุมมอง 3.4K5 หลายเดือนก่อน
Restoring a 1925 Fuller & Johnson 3 1/2 Horsepower engine that was seized and missing many parts. I show before and after as well as the many obstacles encountered and how they were overcome to restore the engine.
Homemade Wet Sharpener made from garbage disposal
มุมมอง 3.1K5 หลายเดือนก่อน
I made a wet sharpener from a garbage disposal I dug out of the neighbor trash.
Homemade rock polisher made from a garbage disposal.
มุมมอง 2185 หลายเดือนก่อน
Homemade rock polisher made from a garbage disposal.
Homemade trusses built with bearing press
มุมมอง 8K6 หลายเดือนก่อน
Homemade trusses built with bearing press
Bicycle fork straightening tool made at home.
มุมมอง 3.8K6 หลายเดือนก่อน
Bicycle fork straightening tool made at home.
Homemade brake system pressure bleeder used on a Toyota FJ40 Landcruiser.
มุมมอง 2086 หลายเดือนก่อน
Homemade brake system pressure bleeder used on a Toyota FJ40 Landcruiser.
Homemade valve lifter and pushrod storage rack for a Toyota FJ40 Landcruiser
มุมมอง 826 หลายเดือนก่อน
Homemade valve lifter and pushrod storage rack for a Toyota FJ40 Landcruiser
Installation of the harmonic balancer on a Toyota FJ40 Landcruiser
มุมมอง 996 หลายเดือนก่อน
Installation of the harmonic balancer on a Toyota FJ40 Landcruiser
Removing the timing gear on a Toyota FJ40
มุมมอง 1246 หลายเดือนก่อน
Removing the timing gear on a Toyota FJ40
Installing timing gear on the crankshaft of a Toyota FJ 40 Landcruiser
มุมมอง 606 หลายเดือนก่อน
Installing timing gear on the crankshaft of a Toyota FJ 40 Landcruiser
Removing harmonic balancer Toyota FJ 40
มุมมอง 2636 หลายเดือนก่อน
Removing harmonic balancer Toyota FJ 40
Removing a Toyota FJ40 transmission that is stuck to the engine.
มุมมอง 4126 หลายเดือนก่อน
Removing a Toyota FJ40 transmission that is stuck to the engine.
Excellently engineered solution, sir.
Subbed and bell on! Your voice and demeanor were made for showing folks how - to's. You're also a smart guy, I enjoy watching your creations.
Jim, Thanks for the kind feedback, really appreciate you watching and subscribing, Kevin
Amen
Don, appreciate the comment and thanks for watching, Kevin
Any milling at all on a drill press is dangerous without a drawbar to secure the taper on the chuck & i would not have any milling cutters in a drill chuck it will come loose even light milling, get your self a mill & be safe.
Appreciate your sharing this, safety is important!
Excellent work. We shared this video on our homemade tool forum last week 😎
Appreciate the feedback, thanks for sharing on your forum. I really enjoy these types of projects, Kevin
@@kevins_fix-it_or_make-It_shop Yeah, building the tools is often more satisfying than using them.
A really good idea! Above all, it can be dismantled.
I appreciate the feedback, works great when you occasionally need that ability. Thanks for watching, Kevin
I have a 12” model that I am rebuilding. It is mostly in good shape.
Nice job!
Danny, Appreciate the feedback, thanks for watching, Kevin
Nice setup Mr. Kevin! I've been wanting to do something like this for a while. I like how you did this. I have 4 lathes but not a mill. I guess I should stop buying lathes and find me a milling machine... Thanks for sharing, I subbed!
Danny, thank you! Kevin
Simples, e eficiente! Good…
Grazie, Kevin.
Very ingenious, good job! My depth stop was very low quality and was not accurate whatsoever so I removed it completely. Has anyone seen a diy version that might work on my 9” unit?
I appreciate the feedback, thanks for watching!
Amazing
Thanks
Really smart upgrades. Paint the switch knob R E D .
I can't wait to see what you post next, but I have no doubt it'll be fun to watch. Thanks for sharing
Really appreciate your feedback, thanks for watching, Kevin
It's a well built for a Ryobi. Most of their tools barely have any metal.
Bob, The Ryobi saw is an older model, I was surprised how solid is. Regards, Kevin
Nice upgrades. I have a brother to your press. Bought it for $100 in 1968.
Appreciate the feedback, amazing yours is a 1968! Thanks for watching, Kevin
Nice work. I love the outro by the way. Shows pride in your work by showing the cleaning up and it also kinda says “job well done”. Kudos!
Mark, I appreciate the comments, it is a homage to my dad, he taught me to put tools away and clean up. Thanks for watching, Kevin
@@kevins_fix-it_or_make-It_shop The world needs more men like you!
@@mark_luna Mark, thank you! Kevin
Love that switch mod!
Mark, I appreciate the feedback, thanks for watching! Kevin
I would replace that keyed chuck with the keyless chuck… they’re not that expensive.
I appreciate the tip, that would save a lot of time, thanks for watching! Kevin
What brand and where to find it, if you don’t mind🙂
Nice device to have! Thank you for sharing this video.
Lonnie, appreciate the comment, thanks for watching, Kevin
I like that switch arrangement. I have a similar setup. I think I’m going to use a tandem switch, one throw for the motor, one for the light.
John, thanks for taking the time to comment, like your tandem switch idea, Kevin
Brillant! - an informative, nicely explained and useful video - I like the speed change lever idea and will use a version of it on my drill press Well done and thank you! :)
Hi, appreciate your feedback, glad the video helped, thanks for watching, Kevin
No probs - nicely explained and demonstrated, unlike some on here! Best wishes. @@kevins_fix-it_or_make-It_shop
Upper part of the shaft of my drill press (cheap Chinese) is responsible for 90% of spindle play. Do you have any drawings or photos of such assembly?
Hi, I don't have any drawings of my drill press and don't see a way to send you a picture of my drill press through this email portion of TH-cam. My drill press seems tight and I do not have any play in the spindel. The lower portion supported by a large ball bearing, upper portion I can not see, but most likely is a sleeve bearing of some kind. Not much help to you, Kevin
Those are all great upgrades.
Dustin, I appreciate your feedback, thanks for watching my video, Kevin.
I have this same machine in my shop from the 80s. It has been a good machine & my hands use it almost without the engagement of my mind. One upgrade on mine was to replace the original set-screw in the channel that allows the table to tilt. Mine now has a permanent set that can be altered if ever I want to tilt the table. Before, it tended to tilt of its own accord. I have several drill presses now, better ones, yet I go back to this one the most.
James, thanks for watching and commenting. Some simple changes can make a big difference, Kevin
Large trusses are built with structural old growth lumber only which is typically 3X as strong as lumberyard material. Unless the building span is very small I would not recommend anyone building their own trusses. I am an engineer,
Tim, I appreciate your feed back, the span was small for a storage shed. Thanks for watching, Kevin
Nice saw and mods. I love vintage craftsman saws. I had an old 10" cabinet tablesaw that was a beauty
Nice job, the only comment I have is the Technium had a rear steel triangle and the front triangle is aluminum, so the lugs were glued where the steel and aluminum come together. They did have some frame failures with this method, so check carefully for any paint cracking on the lugs.
Thanks for the feedback! Really good information, I checked the frame over very carefully and found no cracks in paint or any evidence of stress on the frame. Really appreciate it Kevin.
Nice work. I’m going to have to look you up.
Nice project!
Awesome idea. Thanks for the inspiration
Robert, I appreciate your feedback. Thanks for watching, Kevin
I purchased the same drill press in 1982. I love it and use it all the time. My looks a lot more rustic than yours. Perhaps it is time to clean it up.
Appreciate your comments! My dad and I bought the drill press at a business that was importing power tools back then, this was before we had stores like Harbor Freight. It was a tremendous savings and value. Thanks for watching, Kevin.
I was born in 1986😂... but on a little more serious note. I currently have 4 Drill Presses, the "youngest" is a Startrite Floor Type (Made in England) from 1998, then I have a very small bench model dating from 1982 (Taiwanese made), another bench model (Japanese) from 1979 and a huge bench type (Also made in Japan, but different manufacturer). This last one is pre 1966, but not sure which year exactly. Weighs in around 140kg (+/-300lbs). Build quality on the older machines are much better than anything new available from China nowadays.
Cool idea I was going to ask, you can't do top and bottom nail plates at the same time can you?
I appreciate the feedback, it may be possible. I found it was easier to focus on the one side and get all the joints tight, positioned and the truss plate placed correctly. Once the one side is done it was quick easy to do the other side with everything locked in place. Thanks for watching, Kevin.
Cool! Looks pretty good! When will we get to see it run?
I appreciate the feedback! I plan in doing a prep, start and run video of this engine when we get past the snow and mud season. Thanks for watching, Kevin.
Enjoyed your video but a bit disappointed not to hear it run.
David, I appreciate your feed back! I plan to do a Prep, Start and Run video on the engine when the weather improves and we are past the snow and mud season.Thanks for watching, Kevin
Awesome work, I see you are running a buzz coil yet that looks like a complete magneto because I see a horseshoe magnet, Was the coil part too far gone?
Thank you, the engine has has some interesting modifications in its life. The top of the magneto was cut off, just leaving the lower housing and points and using a 6 volt coil for ignition. It looked really bad, so I made an arched cover to make look better. Thanks for your interest and watching the video, Kevin.
Awesome
Thanks so much, Kevin
beautifull restoration!
Thank you very much, appreciate your feedback, Kevin
Very nice work. I just really like old engines
Thank you very much, I love them too, Kevin
Great videos on the 40 . tip , important to grease threads on any threaded puller threads before use , if not under load threads may gall and seize sometimes damaging it beyond repair . greased threads also makes it easier to turn . i used a white calcium zinc based anti seize on all mine but any grease on hand will be better than nothing .
Yes, very good tip! Thanks for your feedback, Kevin
off of a Coldwell reel mower!. sadly is not a hit and miss but throttle governed engine very cool engine none the less!
Yes, we had a Coldwell mower when I was young, it was a beast. For fun I called this engine a Hit and Can't miss because it doesn't miss a beat. Thanks for your comments and watching the video, Kevin
Woah, cool info. I'm glad you recognized it because I thought this was a small marine engine, because of the long shaft.
You did a great job. Looks fantastic.
Thanks so much!
Good video, really enjoyed it, nice job
Thank you very much!
good for another 99 years, very nice job, I felt I would have liked to see it run, but then again it's done enough work. Let it rest and just look good.
Darryl, Thanks for your feedback. I plan on doing a video on starting and running this engine. Waiting to get out of mud season and better weather! Thanks for watching, Kevin
That answers my question from the grinder video (which I saw first), about having the wheel recessed below the top of the enclosure to capture the water droplets. How well does that end up working anyway? Does it catch everything, or do a few droplets still escape? Also, using the same device to polish rocks AND grind chisels, just by swapping out the wheel, is brilliant. Double the use, for only a little bit more engineering! So, have you ever had/used a metal lathe or milling machine? I think you'd make great use of, and really enjoy using, those to make stuff. ...Just don't get sucked in to starting with one of those crummy little 7×## mini lathes. Keep your eyes open for an older lathe that has a Back Gear for decent torque at low speeds. (I started with a little Atlas model 618 - also commonly rebranded and sold under the Craftsman name - and have never looked back.) Cheers!
Douglas, Thanks for your comments and feedback. I was expecting some overspray, but amazingly there was none. The grinding wheel is about 1/8" below the housing and it is able to catch and direct the water downward. You are so right about lathes. I have a 1947 Logan and it is very basic but rock solid. Thanks again, Kevin
That's a really great idea! I've wondered about how you're supposed to get those plates on without smashing the little pins over sideways. You remind me a lot of the kinds of things my dad used to come up with. He made similar kinds of devices from whatever he had on hand at the time. Sometimes they looked a bit like Rube Goldberg devices that I never would have imagined - but every one of them did exactly what he wanted them to do. I'm looking forward to seeing more build ideas from you. +1 new subscriber.
Excellent build. Thank you for sharing.
Great job of a excellent idea.Thanks for the video for a future project for me.
Congratulations on a successful Fix-it! It looks as though the crash that caused the damage bent the fork only and not the frame top and down tubes. This suggests that the fork tubes were on the light side and would need careful checking for any damage other than the bend eg cracks in brazed joints, fork crown or tubes. It would also be a good idea to check the steerer; traditionally, the joint between steerer and for crown could fail in service and cause a nasty accident.
Very nice and compact unit. I'd suggest putting a SCR on it to reduce the rpm. A simple cheap one from the Chinaman would do. ;)