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Kevin's Fix-it or Make-it Shop
United States
เข้าร่วมเมื่อ 13 ก.ค. 2016
Fix-It or Make-it projects, Homemade tools, Toyota FJ40 Landcruiser repairs.
Vintage Craftsman Bandsaw Tune Up.
I bought a Vintage Craftsman Bandsaw that had a bad sound when running, I show how I was able to tune it up and make run smooth and quiet!
มุมมอง: 108
วีดีโอ
Found a Free Bostich compressor and I Fixed it!
มุมมอง 9721 วันที่ผ่านมา
I found a Bostich compressor in the trash and Fixed it.
Homemade buffer made from a garbage disposal!
มุมมอง 466หลายเดือนก่อน
I found a garbage disposal and turned it into a homemade buffer!
Found and Fixed -I Found and Fixed a Lesco Commercial Fertilizer Spreader!
มุมมอง 111หลายเดือนก่อน
I found a Lesco commercial fertilizer spreader in the trash and fixed it up!
Homemade Sickle Bar Mower for Sub Compact Tractor.
มุมมอง 1.3K2 หลายเดือนก่อน
I built a sickle bar mower for my sub compact tractor from an 1960's 4' sickle bar and designed a scaled down version of a 3 point hitch and drive system.
Homemade Fertilizer Spreader for a Sub Compact Tractor
มุมมอง 5362 หลายเดือนก่อน
I made a 3 point hitch mounted fertilizer spreader for my sub compact tractor. I used a push spreader that I found in the trash and built a frame and used a right angle drill accessory to drive the distribution rotor.
1925 Fuller & Johnson 3 1/2hp Model L start up and running of this 100 year old engine.
มุมมอง 3642 หลายเดือนก่อน
I restored a 1925 Fuller and Johnson 3 1/2 motor and I show the prep, start and running of this 100 year old engine.
Toyota Fj40 Fuel Pump Retro Mod Makeover.
มุมมอง 945 หลายเดือนก่อน
I took newer style Toyota FJ40 fuel pump and modified it to have the features of the original early fuel pumps with serviceable valves and manual priming.
Drill Press Homemade Upgrade-Precision Spindle/Milling Head control.
มุมมอง 23K6 หลายเดือนก่อน
I turned my vintage drill press into milling machine by making a precision spindle height attachment.
Homemade upgrade to a budget Cross Slide Vise for a drill press.
มุมมอง 6176 หลายเดือนก่อน
Bought a budget Cross Slide Vise and it had some play in both axis. I made some simple shims that increased its accuracy remarkably.
Homemade self-cleaning filter for ditch/lake pump intake.
มุมมอง 1966 หลายเดือนก่อน
I built an intake filter on my ditch that automatically cleans itself by using an internal rotating sprinkler. Could be used on a lake or other pump intake filter needs.
Trash to Treasure-Ryobi Circular Saw
มุมมอง 3837 หลายเดือนก่อน
I found a Ryobi Circular Saw in someone's trash. I was able to fix by making a a small homemade part.
Trash to Treasure- Ryobi Hedge Trimmer
มุมมอง 3407 หลายเดือนก่อน
I found a Ryobi Hedge Trimmer in someone's trash and repaired it and adapted it to use a Dewalt 20 volt battery.
Trash to Treasure Dyson Animal Vacuum
มุมมอง 607 หลายเดือนก่อน
I found a Dyson Animal Vacuum in someone's trash, it was easily repaired by finding a clog in it.
Rescued and Repaired DYSON VACUUM sucks up 40 pounds of bricks!
มุมมอง 958 หลายเดือนก่อน
I rescued this vacuum from the trash and repaired it and wanted to come up with a way to show how powerful it is, so I made a vacuum actuator to see how much weight it would lift. Its a beast!
Homemade Power Tool Stand from a shipping crate.
มุมมอง 3369 หลายเดือนก่อน
Homemade Power Tool Stand from a shipping crate.
Homemade Electric Lift is a back saver!
มุมมอง 1.1K9 หลายเดือนก่อน
Homemade Electric Lift is a back saver!
Vintage Radial Arm Saw with Homemade upgrades still can Cut It!
มุมมอง 1.4K9 หลายเดือนก่อน
Vintage Radial Arm Saw with Homemade upgrades still can Cut It!
Vintage Drill Press Homemade Upgrades
มุมมอง 17K9 หลายเดือนก่อน
Vintage Drill Press Homemade Upgrades
Homemade wood auger bit rack made out of lawn edging.
มุมมอง 38110 หลายเดือนก่อน
Homemade wood auger bit rack made out of lawn edging.
Restoring 100 year old Engine Hit and Can't Miss!
มุมมอง 3.5K10 หลายเดือนก่อน
Restoring 100 year old Engine Hit and Can't Miss!
Homemade Wet Sharpener made from garbage disposal
มุมมอง 3.2K10 หลายเดือนก่อน
Homemade Wet Sharpener made from garbage disposal
Homemade low cost lapidary polisher made from a garbage disposal.
มุมมอง 25611 หลายเดือนก่อน
Homemade low cost lapidary polisher made from a garbage disposal.
Homemade trusses built with bearing press
มุมมอง 10K11 หลายเดือนก่อน
Homemade trusses built with bearing press
Bicycle fork straightening tool made at home.
มุมมอง 4.3K11 หลายเดือนก่อน
Bicycle fork straightening tool made at home.
Homemade brake system pressure bleeder used on a Toyota FJ40 Landcruiser.
มุมมอง 31311 หลายเดือนก่อน
Homemade brake system pressure bleeder used on a Toyota FJ40 Landcruiser.
Homemade valve lifter and pushrod storage rack for a Toyota FJ40 Landcruiser
มุมมอง 11711 หลายเดือนก่อน
Homemade valve lifter and pushrod storage rack for a Toyota FJ40 Landcruiser
Installation of the harmonic balancer on a Toyota FJ40 Landcruiser
มุมมอง 22311 หลายเดือนก่อน
Installation of the harmonic balancer on a Toyota FJ40 Landcruiser
Removing the timing gear on a Toyota FJ40
มุมมอง 28311 หลายเดือนก่อน
Removing the timing gear on a Toyota FJ40
Installing timing gear on the crankshaft of a Toyota FJ 40 Landcruiser
มุมมอง 9411 หลายเดือนก่อน
Installing timing gear on the crankshaft of a Toyota FJ 40 Landcruiser
WoW I have that exact same saw. The gold colored ones are from the very early 1960's (1960-1962) era. Love mine and love all the things it can do.
It is dangerous to mill with a drill press because the jaw cone is not fixed and it can escape, moreover the bearings are not designed to work horizontally and lastly it will never do a good job because a drill press is not rigid enough
I made this to accomplish a specific lightweight milling project, I needed to mill a small area of an aluminum valve body for a fuel pump, which I show in another video. Using the dial indicator made the milling an easy task and I was able to mill the aluminum very accurately. The milling was done with a large cross slide vise and a heavy milling plate which acts a a safety device keeping the chuck from dropping down no more than an inch, the chuck would need to drop more than three inches to be thrown free of the drill press. Kevin
To make it safer to use put the chuck guard back on.
I have one exactly like it. Bought it brand new. Still works great. By the way you did a good job of explaining the adjustments.
Thanks for making this, I had the exact same idea but wondered if it would work, or if I was just going to waste time…. This clinched it for me, now I know how to proceed, hanks so much!
Your welcome! Appreciate the feedback, Kevin
This is great! I have had old disposals but never could figure out what to use them for.
Glad it gave you some ideas, thanks for watching! Kevin
Nice, I like the simple method. Not a wide range, not the whole range of travel of the spindle, but for an inch or so of travel not bad. You have a way to adjust the table height, a crude adjustment with the rack and pinion that came with the press. Overall not bad.
I appreciate that you put your tools back where they belong!
Great work; this is a rarely made tractor attachment. We shared this video on our homemade tool forum last week 😎
Appreciate your comments and sharing the video with your forum. Thank you, Kevin.
Good work. We shared this video on our homemade tool forum last week 😎
Thanks homemade tools! Appreciate your feedback and posting my video to your forum, Kevin
Well Done & Well Presented.
I appreciate your feedback, thanks for watching the video! Kevin.
can you tell me how far apart the 2 bolt holes are in the balancer, thanks my puller is 3-1/2 " center to center,
Hi, I measured mine and it is 3 1/2". Thanks for watching the video, Kevin
Hi Kevin, hopefully you see this ,does the magneto come of the face plate ,there must be a shaft for the bushing to be frozen, this is were I'm at right now ,I'm hoping that's all I find frozen, and were you able to use the existing magneto or is that why you used the buzz coil. Any help is more than much applicated ,Thank you even if you can't respond I do appreciate the video .
My magneto was chopped off and just the lower part was left where the cam and points are housed, it was converted to run on a battery and I went with that. My magneto base mounts to a horizontal plate that is part of the cast iron side face plate. The magneto gear that is driven by the larger cam gear has to be removed also to be able to remove the magneto completely from the side plate as well. My magneto was also the main reason for the engine not turning . Once I removed the magneto I had some movement in the piston. It took quite a bit of effort to free up the magneto bearing itself. Lot of lubrication and gently working the shaft back and forth. Hope this helps in some way. Kevin
@@kevins_fix-it_or_make-It_shop Thank you ,the rust poors out the little hole in the front of my magneto ,I have the little transmission freed up,qnd the governor ,the piston and valve have been soaking scene the day I committed here ,I had just bought and drove back the 150 miles to pick it up,I'm going to brave up and remove the front plate tonight ,I believe the magneto is the reason it's frozen,I'll probably find out the hard way nothing ever goes easy for me,plan on using this motor for a 1904 de dion Bouton buggy build ,I know this was a reel mower engine, but it so close to those early car motors I love to see it run again if possible, hope you have a wonderful day ,and Thanks so much.
Like the video. I've been looking how to make my own trusses and floor joists haven't found the perfect hydraulic c press yet but just and idea that might save you time on keeping everything aligned try using a corregated fasner stapler.
Ha I have the exact same drill press just a lower model as it’s missing the light
I just bought one like this today, it has everything including the original radiator motor is frozen, I'll be watching this video a lot as I'll try and restore it😊
So great you got the radiator! Mine was frozen also, I disconnected the connecting rod from crankshaft and removed the cylinder from the crankcase. I worked on the cylinder below the piston and got it cleaned up with a small hone. was able to draw out the piston from the cylinder. Good luck and thanks for watching! Kevin
Ton travail merveilleux il lui manque les plans de mesure pour que tes abonnée réalisant ton idée chez soit
Merci d'avoir regardé ! La vidéo montre uniquement un concept. Chaque perceuse à colonne est différente et les plans et les mesures ne s'appliqueraient pas à tous les modèles de perceuse à colonne fabriqués. Kévin
Very well done! Ingenuity!
Gracias por la opcion me ayuda mucho para las personas q no podemos tener una fresadora genial.
Very nice upload mo new ideas how work can we do with drill press
Appreciate the feedback, Thanks for watching!
Fantástico.A melhor ideia que eu vi até hoje.
I like your very clever setup Only problem; drill presses make very poor milling machines.
Thanks for watching and commenting! This setup ended up working surprisingly well. I wanted to mill an aluminum valve body for a fuel pump and it turned out to work well and allowed me to precisely mill my project. I know it has limited ability but it did what I needed. Thanks, Kevin
Nice tips. I would paint that on/off switch red.
Thanks, red is a good idea, Kevin
Verry nice.
I appreciate that, thanks for watching, Kevin
It looks similar in build quality to my 1956 DeWalt MB RAS which is also pretty much all cast iron, mine's only drawback being that it takes a 9" blade, which, while they can be found are nowhere near as prolific as the 10" blades. Mine has a toggle on/off switch closer to the base of the arm on its right side which I am happy with. Never cared for those keyed switches, which, whenever I've had them, I super glue the key in place so there's never any chance of losing it.
❤❤❤ veri veri god
Excellently engineered solution, sir.
Thanks for your comment, I was really relieved when it popped loose! Kevin
Subbed and bell on! Your voice and demeanor were made for showing folks how - to's. You're also a smart guy, I enjoy watching your creations.
Jim, Thanks for the kind feedback, really appreciate you watching and subscribing, Kevin
Amen
Don, appreciate the comment and thanks for watching, Kevin
Any milling at all on a drill press is dangerous without a drawbar to secure the taper on the chuck & i would not have any milling cutters in a drill chuck it will come loose even light milling, get your self a mill & be safe.
Appreciate your sharing this, safety is important!
Excellent work. We shared this video on our homemade tool forum last week 😎
Appreciate the feedback, thanks for sharing on your forum. I really enjoy these types of projects, Kevin
@@kevins_fix-it_or_make-It_shop Yeah, building the tools is often more satisfying than using them.
A really good idea! Above all, it can be dismantled.
I appreciate the feedback, works great when you occasionally need that ability. Thanks for watching, Kevin
I have a 12” model that I am rebuilding. It is mostly in good shape.
Nice job!
Danny, Appreciate the feedback, thanks for watching, Kevin
Nice setup Mr. Kevin! I've been wanting to do something like this for a while. I like how you did this. I have 4 lathes but not a mill. I guess I should stop buying lathes and find me a milling machine... Thanks for sharing, I subbed!
Danny, thank you! Kevin
Simples, e eficiente! Good…
Grazie, Kevin.
Very ingenious, good job! My depth stop was very low quality and was not accurate whatsoever so I removed it completely. Has anyone seen a diy version that might work on my 9” unit?
I appreciate the feedback, thanks for watching!
Amazing
Thanks
Really smart upgrades. Paint the switch knob R E D .
Absolutely going to make one for my 42' Craftsman DP. Yes, the knob will be red. Great idea!
I can't wait to see what you post next, but I have no doubt it'll be fun to watch. Thanks for sharing
Really appreciate your feedback, thanks for watching, Kevin
It's a well built for a Ryobi. Most of their tools barely have any metal.
Bob, The Ryobi saw is an older model, I was surprised how solid is. Regards, Kevin
Nice upgrades. I have a brother to your press. Bought it for $100 in 1968.
Appreciate the feedback, amazing yours is a 1968! Thanks for watching, Kevin
Nice work. I love the outro by the way. Shows pride in your work by showing the cleaning up and it also kinda says “job well done”. Kudos!
Mark, I appreciate the comments, it is a homage to my dad, he taught me to put tools away and clean up. Thanks for watching, Kevin
@@kevins_fix-it_or_make-It_shop The world needs more men like you!
@@mark_luna Mark, thank you! Kevin
Love that switch mod!
Mark, I appreciate the feedback, thanks for watching! Kevin
I would replace that keyed chuck with the keyless chuck… they’re not that expensive.
I appreciate the tip, that would save a lot of time, thanks for watching! Kevin
What brand and where to find it, if you don’t mind🙂
Nice device to have! Thank you for sharing this video.
Lonnie, appreciate the comment, thanks for watching, Kevin
I like that switch arrangement. I have a similar setup. I think I’m going to use a tandem switch, one throw for the motor, one for the light.
John, thanks for taking the time to comment, like your tandem switch idea, Kevin
Brillant! - an informative, nicely explained and useful video - I like the speed change lever idea and will use a version of it on my drill press Well done and thank you! :)
Hi, appreciate your feedback, glad the video helped, thanks for watching, Kevin
No probs - nicely explained and demonstrated, unlike some on here! Best wishes. @@kevins_fix-it_or_make-It_shop
Upper part of the shaft of my drill press (cheap Chinese) is responsible for 90% of spindle play. Do you have any drawings or photos of such assembly?
Hi, I don't have any drawings of my drill press and don't see a way to send you a picture of my drill press through this email portion of TH-cam. My drill press seems tight and I do not have any play in the spindel. The lower portion supported by a large ball bearing, upper portion I can not see, but most likely is a sleeve bearing of some kind. Not much help to you, Kevin
Those are all great upgrades.
Dustin, I appreciate your feedback, thanks for watching my video, Kevin.